| Date: | Sunday 2 June 1996 |
| Time: | 14:12 LT |
| Type: | Shorts 360-300 |
| Owner/operator: | Gulfstream International Airlines |
| Registration: | N826BE |
| MSN: | SH3745 |
| Year of manufacture: | 1988 |
| Total airframe hrs: | 10953 hours |
| Engine model: | P&W PT6A-67R |
| Fatalities: | Fatalities: 0 / Occupants: 35 |
| Other fatalities: | 0 |
| Aircraft damage: | None |
| Category: | Serious incident |
| Location: | Miami, FL -
United States of America
|
| Phase: | Initial climb |
| Nature: | Unknown |
| Departure airport: | (KMIA) |
| Destination airport: | Orlando, FL (KMCO) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The captain stated that the elevator trim worked fine during preflight inspection, and was set for takeoff. With the first officer flying the airplane after takeoff, while climbing through 300 feet, the elevator trim cable failed. The captain assisted the first officer, and the flight returned and landed uneventfully. Examination of the airplane revealed that an elevator trim cable failed due to fatigue about 18 inches forward of a turnbuckle and just aft of a pulley where a 45-degree change in direction occurred. The cable was required to be inspected every 1,460 days or 4,800 hours. At the time of the failure, the cable had accumulated 1,679.4 hours and 2,017 cycles, since last inspection 573 days earlier, and a total of 10,953.0 hours and 16,193 cycles, since new.
Probable Cause: fatigue failure of a segment of the elevator trim cable.
Accident investigation:
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|
| | |
| Investigating agency: | NTSB |
| Report number: | MIA96IA146 |
| Status: | Investigation completed |
| Duration: | 1 year and 2 months |
| Download report: | Final report
|
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Sources:
NTSB MIA96IA146
Location
Revision history:
| Date/time | Contributor | Updates |
| 13-Mar-2024 16:27 |
ASN Update Bot |
Added |
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