| Date: | Saturday 29 April 1995 |
| Time: | 18:30 LT |
| Type: | Beechcraft B95 |
| Owner/operator: | Private |
| Registration: | N9902R |
| MSN: | TD-422 |
| Total airframe hrs: | 5094 hours |
| Engine model: | Lycoming O-360-A1A |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Leakesville, MS -
United States of America
|
| Phase: | Approach |
| Nature: | Private |
| Departure airport: | |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE FLIGHT LOST POWER IN BOTH ENGINES WHILE ON FINAL APPROACH FOR A TOUCH-AND-GO LANDING. POSTCRASH EXAMINATION OF THE ENGINE ASSEMBLIES AND ACCESSORIES SHOWED NO EVIDENCE OF PRECRASH MECHANICAL FAILURE OR MALFUNCTION. THE AIRCRAFT'S FUEL SELECTORS WERE FOUND IN THE MAIN TANK POSITION. THE UNDAMAGED LEFT MAIN FUEL TANK CONTAINED 7 GALLONS OF FUEL. THE RIGHT TANK WAS DAMAGED IN THE ACCIDENT AND WAS FOUND EMPTY. EACH CARBURETOR DID NOT CONTAIN FUEL. THE BEECH B95 AIRCRAFT IS RESTRICTED FROM TAKING OFF WITH LESS THAT 13 GALLONS IN EACH MAIN TANK TO PREVENT FUEL INTERRUPTION TO THE ENGINES.
Probable Cause: THE FAILURE OF THE PILOT-IN-COMMAND TO OPERATE THE AIRCRAFT IN ACCORDANCE WITH MANUFACTURER'S LIMITATIONS RESULTING IN FUEL STARVATION AND A TOTAL LOSS OF POWER IN BOTH ENGINES.
Accident investigation:
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|
| | |
| Investigating agency: | NTSB |
| Report number: | MIA95LA123 |
| Status: | Investigation completed |
| Duration: | 3 months |
| Download report: | Final report
|
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Sources:
NTSB MIA95LA123
Location
Revision history:
| Date/time | Contributor | Updates |
| 15-Mar-2024 06:39 |
ASN Update Bot |
Added |
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