| Date: | Sunday 25 September 1994 |
| Time: | 17:20 LT |
| Type: | Cessna 180 |
| Owner/operator: | Private |
| Registration: | N9425C |
| MSN: | 180-31823 |
| Total airframe hrs: | 2565 hours |
| Engine model: | Continental O-470-J |
| Fatalities: | Fatalities: 0 / Occupants: 4 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Denton, TX -
United States of America
|
| Phase: | Approach |
| Nature: | Private |
| Departure airport: | Utopia, TX (95TA) |
| Destination airport: | (5TXO) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING APPROACH TO HIS HOME AIRPORT, THE PILOT EXPERIENCED A COMPLETE POWER LOSS AS HE APPLIED 20 DEG OF FLAPS. HE DETERMINED THAT HE COULD NOT MAKE THE RUNWAY AND ELECTED TO EXECUTE A FORCED LANDING TO A DIRT ROAD. ON SHORT FINAL, THE PILOT SPOTTED POWER LINES AND ENTERED A SHALLOW CLIMB TO CLEAR THEM; HOWEVER, THE RESULTANT LOSS OF AIRSPEED INDUCED A STALL AND THE AIRPLANE IMPACTED THE GROUND. THE PILOT STATED THAT HE BELIEVED A TANK UNPORTED WHEN HE LOWERED THE FLAPS. 5 GALS OF FUEL WERE DRAINED FROM EACH WING TANK DURING RECOVERY. THE FLIGHT MANUAL INDICATED 2.5 GALS PER SIDE IS UNUSABLE.
Probable Cause: THE FUEL STARVATION INDUCED POWER LOSS DUE TO THE PILOT'S FAILURE TO MAINTAIN AN ADEQUATE AMOUNT OF FUEL. FACTORS WHICH CONTRIBUTED WERE: THE LACK OF SUITABLE TERRAIN FOR THE FORCED LANDING, AND THE PILOT'S EVASIVE MANEUVER.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | FTW94LA309 |
| Status: | Investigation completed |
| Duration: | 7 months |
| Download report: | Final report
|
|
Sources:
NTSB FTW94LA309
Location
Revision history:
| Date/time | Contributor | Updates |
| 15-Mar-2024 14:03 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation