| Date: | Saturday 6 August 1994 |
| Time: | 14:00 LT |
| Type: | Cessna 172RG |
| Owner/operator: | Alexandria Aviation, Inc. |
| Registration: | N9686B |
| MSN: | 172RG0967 |
| Total airframe hrs: | 4097 hours |
| Engine model: | Lycoming O-360-F1A6 |
| Fatalities: | Fatalities: 0 / Occupants: 4 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Pittstown, NJ -
United States of America
|
| Phase: | Initial climb |
| Nature: | Unknown |
| Departure airport: | |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRPLANE COLLIDED WITH TREES DURING TAKEOFF FROM ALEXANDRIA AIRPORT ON RUNWAY 8, WHICH IS 2550 FEET LONG. THE PILOT REPORTED THE ENGINE EXPERIENCED A PARTIAL POWER LOSS ON TAKEOFF. HE SAID HE WAS UNABLE TO ESTABLISH A CLIMB AND SETTLED INTO TREES. TWO FAA INSPECTORS OBSERVED THE TAKEOFF AND REPORTED THE AIRPLANE, '...APPEARED TO LIFT OFF EARLY, AT A HIGHER THAN NORMAL PITCH ATTITUDE AND SLOWER THAN NORMAL SPEED. THE AIRCRAFT APPEARED TO MUSH ALONG IN GROUND EFFECT AND NEVER ACCELERATED...ENGINE SOUNDED NORMAL....' IN A WRITTEN REPORT OF POST ACCIDENT EXAMINATION ON THE AIRPLANE AND ENGINE, THE FAA STATED, '...NO ENGINE MALFUNCTIONS COULD BE DETERMINED THAT RESULTED IN A REDUCTION OR LOSS OF POWER TO THE ENGINE....'
Probable Cause: THE PILOT'S PREMATURE LIFT OFF AND FAILURE TO ATTAIN ADEQUATE AIRSPEED.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | NYC94LA151 |
| Status: | Investigation completed |
| Duration: | 5 months |
| Download report: | Final report
|
|
Sources:
NTSB NYC94LA151
Revision history:
| Date/time | Contributor | Updates |
| 15-Mar-2024 17:12 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation