| Date: | Wednesday 27 July 1994 |
| Time: | 17:07 LT |
| Type: | Cessna 140 |
| Owner/operator: | Private |
| Registration: | N9409A |
| MSN: | 15230 |
| Total airframe hrs: | 15544 hours |
| Engine model: | Continental C-90-14F |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Lomax, IL -
United States of America
|
| Phase: | En route |
| Nature: | Private |
| Departure airport: | Grove, OK (1H7) |
| Destination airport: | Moline, IL (KMOL) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT REPORTED HE AND HIS PILOT-RATED PASSENGER WERE FLYING ALONG THE MISSISSIPPI RIVER WHEN THE AIRPLANE STRUCK AN UNSEEN AND UNMARKED POWER LINE. THE AIRPLANE SUBSEQUENTLY WENT INTO THE RIVER, AND THE PILOT AND PASSENGER WERE RESCUED BY BOATERS. ACCORDING TO A POLICE OFFICER WHO INTERVIEWED THE PILOT AND PASSENGER JUST AFTER THE ACCIDENT, THEY SAID THEY WERE JUST FLYING ALONG THE RIVER, WAVING AT PEOPLE AND HAVING FUN. A POWER COMPANY REPRESENTATIVE SAID THE HEIGHT OF THE TWO POLES WHICH SUPPORTED THE POWER LINE WAS ABOUT 60'; HE SAID THE HEIGHT OF THE WIRE WHICH THE AIRPLANE STRUCK WAS APPROXIMATELY 45-50'.
Probable Cause: the pilot's failure to maintain clearance from a transmission wire, and the pilot's failure to maintain an appropriate altitude. A factor associated with the accident is the transmission wire.
Accident investigation:
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| | |
| Investigating agency: | NTSB |
| Report number: | CHI94LA246 |
| Status: | Investigation completed |
| Duration: | 6 months |
| Download report: | Final report
|
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Sources:
NTSB CHI94LA246
Location
Revision history:
| Date/time | Contributor | Updates |
| 15-Mar-2024 17:45 |
ASN Update Bot |
Added |
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