| Date: | Saturday 11 June 1994 |
| Time: | 10:00 LT |
| Type: | Cessna 180H |
| Owner/operator: | Private |
| Registration: | N4764U |
| MSN: | 18051464 |
| Year of manufacture: | 1965 |
| Total airframe hrs: | 2613 hours |
| Engine model: | Continental O-470R |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Wickenburg, AZ -
United States of America
|
| Phase: | Take off |
| Nature: | Private |
| Departure airport: | |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT ATTEMPTED A TAKEOFF WITH THE CONTROL LOCK STILL ENGAGED IN THE CONTROL COLUMN. PHOTOGRAPHS TAKEN BY THE LOCAL SHERIFF SHORTLY AFTER THE ACCIDENT DEPICTED THE CONTROL LOCK STILL INSTALLED.
Probable Cause: the pilot's failure to remove the control lock prior to flight.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | LAX94LA248 |
| Status: | Investigation completed |
| Duration: | 9 months |
| Download report: | Final report
|
|
Sources:
NTSB LAX94LA248
History of this aircraft
Other occurrences involving this aircraft Revision history:
| Date/time | Contributor | Updates |
| 15-Mar-2024 20:33 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation