| Date: | Tuesday 3 May 1994 |
| Time: | 15:30 LT |
| Type: | Cessna 421A |
| Owner/operator: | Private |
| Registration: | N2211W |
| MSN: | 421A-0118 |
| Total airframe hrs: | 3971 hours |
| Engine model: | Continental GTSIO-520-D |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Richlands, VA -
United States of America
|
| Phase: | Landing |
| Nature: | Ferry/positioning |
| Departure airport: | Suffolk County, NY |
| Destination airport: | Grundy, VA (KGDY) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT STATED THAT THE APPROACH WAS NORMAL. HE REPORTED: 'UPON TOUCHDOWN THE NOSE VIBRATED AND WENT FAR BELOW THE NORMAL POSITION. I QUICKLY APPLIED FULL BACK PRESSURE ON THE CONTROL YOKE AND THE MAINS FELL BACK TO THE RUNWAY.' FAA INSPECTORS REPORTED: 'INVESTIGATION...REVEALED EVIDENCE AND AIRCRAFT DAMAGE CONSISTENT WITH HARD LANDING IMPACT WITH RUNWAY SURFACE. PILOT HAD MINIMAL FLIGHT EXPERIENCE IN [THIS] MODEL AIRCRAFT.' BOTH WINGS WERE OBSERVED TO BE BENT DOWN DURING THE EXAMINATION BY THE FAA INSPECTORS. THE PILOT HAD A TOTAL OF 6 HOURS IN THIS MODEL AIRPLANE.
Probable Cause: THE HARD LANDING, AS A RESULT OF THE PILOT'S MISJUDGED RATE OF DESCENT. A FACTOR RELATED TO THE ACCIDENT WAS THE PILOT'S LIMITED EXPERIENCE IN THIS MAKE AND MODEL AIRPLANE.
Accident investigation:
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|
| | |
| Investigating agency: | NTSB |
| Report number: | NYC94LA084 |
| Status: | Investigation completed |
| Duration: | 7 months |
| Download report: | Final report
|
|
Sources:
NTSB NYC94LA084
Location
Revision history:
| Date/time | Contributor | Updates |
| 16-Mar-2024 08:14 |
ASN Update Bot |
Added |
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