| Date: | Friday 17 December 1993 |
| Time: | 14:35 LT |
| Type: | Bellanca 8KCAB |
| Owner/operator: | Private |
| Registration: | N5065G |
| MSN: | 597-80 |
| Total airframe hrs: | 2792 hours |
| Engine model: | Lycoming AEIO-360-H1A |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Westcliffe, CO -
United States of America
|
| Phase: | En route |
| Nature: | Private |
| Departure airport: | |
| Destination airport: | Fremont County, CO |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:AFTER BEING AIRBORNE FOR APPROXIMATELY 2 MINUTES, THE PILOT NOTICED SMOKE ENTERING THE COCKPIT. THIS WAS FOLLOWED BY SEIZURE OF THE ENGINE. THE PILOT CONDUCTED A FORCED LANDING IN MOUNTAINOUS TERRAIN AND ON TOUCH DOWN, THE AIRCRAFT NOSED OVER. THE NUMBER TWO CORRECTING ROD BEARING FAILED AND THE ROD EXITED THROUGH THE ENGINE CASE.
Probable Cause: WAS FAILURE OF THE NUMBER TWO CONNECTING ROD BEARING. A FACTOR WAS UNSUITABLE TERRAIN FOR A FORCED LANDING.
Accident investigation:
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|
| | |
| Investigating agency: | NTSB |
| Report number: | FTW94LA049 |
| Status: | Investigation completed |
| Duration: | 9 months |
| Download report: | Final report
|
|
Sources:
NTSB FTW94LA049
Location
Revision history:
| Date/time | Contributor | Updates |
| 16-Mar-2024 13:34 |
ASN Update Bot |
Added |
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