| Date: | Wednesday 3 November 1993 |
| Time: | 18:11 LT |
| Type: | Beechcraft B36TC |
| Owner/operator: | Tsa Enterprises |
| Registration: | N8006R |
| MSN: | EA-531 |
| Total airframe hrs: | 338 hours |
| Engine model: | Continental TSIO-520-UB |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Rockford, IL -
United States of America
|
| Phase: | Initial climb |
| Nature: | Unknown |
| Departure airport: | (KRFD) |
| Destination airport: | (KRFD) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRPLANE WAS FLOWN ON A CHECK FLIGHT AFTER MAINTENANCE FOR AN OIL-AND-FILTER CHANGE AND REPLACEMENT OF LEAKING GASKETS. DURING THE INITIAL CLIMB AFTER TAKEOFF, THE PILOT NOTED A MOMENTARY LOSS OF POWER, PROMPTING A TURN TOWARDS THE AIRPORT. THE ENGINE LOST ALL POWER IN THE TURN. DURING A LANDING SHORT OF THE RUNWAY, THE AIRPLANE HIT A FENCE. THE MAIN FUEL LINE CONNECTION TO THE FUEL PUMP WAS FOUND LOOSE. WHEN THE BOOST PUMP WAS ENERGIZED, THE LOOSE FITTING LEAKED SUBSTANTIALLY.
Probable Cause: A LOOSE FUEL LINE FITTING, DUE TO IMPROPER MAINTENANCE, WHICH RESULTED IN AN INTERUPTION OF FUEL TO THE ENGINE.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | CHI94LA031 |
| Status: | Investigation completed |
| Duration: | 10 months |
| Download report: | Final report
|
|
Sources:
NTSB CHI94LA031
History of this aircraft
Other occurrences involving this aircraft
| 16 August 2003 |
N93PP |
|
0 |
Temple, Texas |
 |
sub |
| 23 June 2011 |
N93PP |
Arizona Thunderbolts LLC |
0 |
Akron-Colorado Plains Regional Airport, CO (AKO) |
 |
sub |
| CFIT |
Revision history:
| Date/time | Contributor | Updates |
| 16-Mar-2024 14:46 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation