| Date: | Thursday 23 September 1993 |
| Time: | 08:15 LT |
| Type: | Bell UH-1B |
| Owner/operator: | Clearwater Management Co. Inc. |
| Registration: | N3979C |
| MSN: | 62-2048 |
| Year of manufacture: | 1962 |
| Total airframe hrs: | 7922 hours |
| Engine model: | Lycoming T53-L11-D |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Pierce, ID -
United States of America
|
| Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
| Nature: | Unknown |
| Departure airport: | |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WHILE MANEUVERING NEAR A REFUELING SITE IN HILLY/MOUNTAINOUS TERRAIN, THE 90 DEGREE GEARBOX SEPARATED FROM THE AIRCRAFT. THE PILOT THEN ATTEMPTED A RUN-ON FORCED LANDING ON A NEARBY LOGGING ROAD. DURING THE FLARE, THE AIRCRAFT LANDED HARD, RESULTING IN A COLLAPSE OF THE SKIDS, AND SEPARATION OF THE REMAINING PORTION OF THE TAIL BOOM. METALLURGICAL ANALYSIS REVEALED THAT ALL SIX GEARBOX ATTACH BOLTS HAD EXPERIENCED REVERSE-BENDING FATIGUE FAILURE. THE OPERATOR RECORDS INDICATED THAT THIS WAS A NEW SURPLUS PART WHICH HAD 136 HOURS OF OPERATION SINCE NEW. HISTORICAL RECORDS CONFIRMING THE UNIT'S TOTAL TIME SINCE BEING SHIPPED TO THE PHILIPPINES AS A NEW SURPLUS PART IN 1981 COULD NOT BE LOCATED.
Probable Cause: SEPARATION OF THE 90 DEGREE GEARBOX AFTER FATIGUE FAILURE OF THE GEARBOX ATTACH BOLTS. FACTORS INCLUDE HILLY/MOUNTAINOUS TERRAIN.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | SEA93LA207 |
| Status: | Investigation completed |
| Duration: | 1 year |
| Download report: | Final report
|
|
Sources:
NTSB SEA93LA207
Location
Revision history:
| Date/time | Contributor | Updates |
| 16-Mar-2024 16:24 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation