| Date: | Saturday 17 June 1989 |
| Time: | 15:00 |
| Type: | McCulloch J-2 |
| Owner/operator: | private |
| Registration: | N4354G |
| MSN: | 064 |
| Total airframe hrs: | 312 hours |
| Engine model: | Lycoming O-360 |
| Fatalities: | Fatalities: 2 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Destroyed |
| Category: | Accident |
| Location: | Oxford, OH -
United States of America
|
| Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
| Nature: | Private |
| Departure airport: | Shelbyville, IN (35M) |
| Destination airport: | Middletown, OH (MWO) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AUTOGYRO BROKE UP IN FLIGHT WHILE MANEUVERING DURING A PERSONAL FLIGHT. WITNESSES TO THE ACCIDENT REPORTED SEEING THE ROTOR BLADES SLOW AND FOLD UP AS THE AUTOGYRO FLEW SLOWLY OVER A LAKE. ONE ROTOR BLADE WAS SEEN TO SEPARATE FROM THE ROTORHEAD AND FALL SOME DISTANCE FROM THE REST OF THE AIRCRAFT. THE AUTOGYRO THEN CRASHED INTO THE LAKE. INSPECTION OF THE WRECKAGE SHOWED THAT THE MAIN ROTOR MAST THRUST BEARING WAS GALLED AND HAD SEIZED. CAUSE: THE FAILURE OF THE PILOT OPERATOR TO REPLACE THE MAIN ROTOR THRUST BEARING. THE EXPIRED SERVICE LIFE OF THE MAIN ROTOR THRUST BEARING IS A FACTOR IN THE ACCIDENT.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | CHI89FA114 |
| Status: | Investigation completed |
| Duration: | |
| Download report: | Final report
|
|
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001213X28524 Revision history:
| Date/time | Contributor | Updates |
| 24-Oct-2008 10:30 |
ASN archive |
Added |
| 21-Dec-2016 19:22 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency, ] |
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