ASN Wikibase Occurrence # 36199
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Date: | Monday 1 April 1996 |
Time: | 03:58 LT |
Type: | Cessna P210N |
Owner/operator: | Edward Andrews, Jr. |
Registration: | N6427W |
MSN: | P21000776 |
Total airframe hrs: | 1865 hours |
Engine model: | Continental TSIO-520-AF |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Marathon, FL -
United States of America
|
Phase: | Unknown |
Nature: | Executive |
Departure airport: | West Palm Beach, FL |
Destination airport: | (KMTH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During an over-water arrival at night, the pilot reported that the destination airport was in sight, and he canceled his VFR advisories. The controller acknowledged, advised the pilot to squawk 1200, and told him that a frequency change was approved. The pilot acknowledged at 0257:10, then there was no further radio communication with the pilot. At 0257:08, the encoded altimeter showed the airplane was at 1,200 feet, and radar data showed the airplane was descending with a ground speed of 183 to 189 knots. The final radar targets showed the airplane had descended to 200 feet, the heading was about 213 degrees, and the ground speed had increased to nearly 200 knots. Subsequently, the airplane descended into the water about 7 nautical miles north-northeast of the airport. The wreckage was recovered, and examination of the flight controls revealed no evidence of preimpact failure or malfunction. The landing gear and flaps were found retracted. The engine was recovered, and after replacement of components that were not recovered, the engine was started and operated normally. The propeller was recovered almost 1 year and 4 months after the accident; examination of it revealed no evidence of preimpact failure or malfunction. The airplane owner said that at about 1900 hours, before departing on the 1st leg of the flight, the pilot advised that he was tired due to his work/flying schedule. The owner stated that he was not aware that the pilot was going to fly the airplane after that conversation.
Probable Cause: failure of the pilot to maintain sufficient altitude during an over-water approach at night. Factors relating to the accident were darkness and pilot fatigue.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL96FA074 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB ATL96FA074
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:22 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
09-Apr-2024 07:38 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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