| Date: | Sunday 18 April 1993 |
| Time: | 15:30 LT |
| Type: | Avid Flyer |
| Owner/operator: | Private |
| Registration: | N31187 |
| MSN: | 767 |
| Total airframe hrs: | 18 hours |
| Engine model: | ROTAX 582UL |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Winnsboro, SC -
United States of America
|
| Phase: | Initial climb |
| Nature: | Private |
| Departure airport: | |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT REPORTED THAT THE ENGINE LOST POWER AT ABOUT 800 FEET AGL, DURING THE INITIAL CLIMB AFTER TAKEOFF. A 180 DEGREE TURN WAS ACCOMPLISHED AND THE AIRPLANE WAS ALIGNED WITH THE RUNWAY FOR LANDING. ABOUT 60 FEET AGL, OVER THE RUNWAY, THE AIRPLANE STALLED; TOO LOW FOR THE PILOT TO RECOVER. THE AIRPLANE HIT THE GROUND IN A RIGHT WING AND NOSE DOWN ATTITUDE. AN ENTRY WAS FOUND IN THE AIRCRAFT LOG BOOK THAT INDICATED A PREVIOUS ENGINE MALFUNCTION BECAUSE OF A CARBURETOR SETTING THAT WAS TOO LEAN. HOWEVER, AN EXAMINATION OF THE ENGINE FOLLOWING THE ACCIDENT DID NOT REVEAL AN ABNORMALITY, AND THE ENGINE WAS OPERATED AT IDLE POWER.
Probable Cause: The pilot's failure to maintain the airspeed above the stall speed, during the forced landing. A factor was the undetermined engine malfunction.
Accident investigation:
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| | |
| Investigating agency: | NTSB |
| Report number: | ATL93LA077 |
| Status: | Investigation completed |
| Duration: | 1 year and 2 months |
| Download report: | Final report
|
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Sources:
NTSB ATL93LA077
Location
Revision history:
| Date/time | Contributor | Updates |
| 17-Mar-2024 18:40 |
ASN Update Bot |
Added |
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