| Date: | Saturday 8 August 1992 |
| Time: | 23:15 LT |
| Type: | Air Tractor AT-401 |
| Owner/operator: | Morris, Gary & Connie |
| Registration: | N1547P |
| MSN: | 401-0861 |
| Total airframe hrs: | 273 hours |
| Engine model: | P&W R-1340-AN1 |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Parker, AZ -
United States of America
|
| Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
| Nature: | Agricultural |
| Departure airport: | |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT WAS CONDUCTING AN AERIAL APPLICATION SWATH RUN WHEN 10 INCHES OF A PROPELLER BLADE SEPARATED. THE PILOT EXECUTED AN EMERGENCY LANDING. ON TOUCHDOWN, THE AIRCRAFT NOSED OVER AFTER COLLIDING WITH THE ROUGH/UNEVEN TERRAIN. A METALLURGICAL EXAMINATION OF PROPELLER BLADE DISCLOSED THE PRESENCE OF FATIGUE ACROSS 60% OF THE FRACTURED SURFACE. THE ORIGIN OF THE FATIGUE CENTERED ON A NOTCH OF A PREVIOUSLY REWORKED AREA. THE PROPELLER BLADE HAD ACCURED 273 FLIGHT HOURS SINCE IT WAS OVERHAULED.
Probable Cause: THE INADEQUATE OVERHAUL OF THE PROPELLER BLADE BY THE OVERHAUL FACILITY. CONTRIBUTING TO THIS ACCIDENT WAS THE ROUGH AND UNEVEN TERRAIN.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | LAX92LA338 |
| Status: | Investigation completed |
| Duration: | 1 year |
| Download report: | Final report
|
|
Sources:
NTSB LAX92LA338
History of this aircraft
Other occurrences involving this aircraft
| 15 February 2023 |
HK-4077 |
Fumigaray |
0 |
La Lucha (SKGM), Ciénaga |
 |
sub |
| Mid-air collision |
Location
Revision history:
| Date/time | Contributor | Updates |
| 18-Mar-2024 14:08 |
ASN Update Bot |
Added |
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