| Date: | Sunday 20 October 1991 |
| Time: | 15:00 LT |
| Type: | Quickie Q2 |
| Owner/operator: | Atakan Sabay |
| Registration: | N82BD |
| MSN: | 2546 |
| Engine model: | REVMASTER 2100-D |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Arcola, TX -
United States of America
|
| Phase: | Landing |
| Nature: | Private |
| Departure airport: | (KAXH) |
| Destination airport: | (KAXH) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING A DAYTIME APPROACH, THE PILOT LOST CONTROL OF THE AIRPLANE DURING THE LANDING ROLL. THE AIRPLANE PORPOISED AND VEERED LEFT OFF THE RUNWAY AND NOSED OVER INTO THE INVERTED POSITION. THE PILOT REPORTED ENGINE ROUGHNESS AND AIRPLANE INSTABILITY; HOWEVER, NO DISCREPANCIES WITH AIRPLANE CONTROLS NOR THE ENGINE WERE FOUND AT THE TIME OF THE INVESTIGATION. THE PILOT FURTHER REPORTED THAT THERE WAS NO INTENT TO FLY AND THAT HE GOT AIRBORNE INADVERTENTLY DURING AN INTENDED HIGH SPEED TAXI. THE COWL FLAP WAS LEFT TAPED SHUT. THE ACCIDENT OCCURRED ON THE THIRD ATTEMPTED LANDING.
Probable Cause: THE PILOT'S IMPROPER FLARE AND IMPROPER RECOVERY FROM THE RESULTANT BOUNCED LANDING. A FACTOR WAS THE PILOT'S LACK OF FAMILIARITY WITH THE AIRPLANE.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | FTW92LA018 |
| Status: | Investigation completed |
| Duration: | 1 year and 6 months |
| Download report: | Final report
|
|
Sources:
NTSB FTW92LA018
Location
Revision history:
| Date/time | Contributor | Updates |
| 19-Mar-2024 13:56 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation