| Date: | Tuesday 27 August 1991 |
| Time: | 14:00 LT |
| Type: | Piper PA-32R |
| Owner/operator: | Barron Thomas Aviation, Inc. |
| Registration: | N9222K |
| MSN: | 32R-7680197 |
| Engine model: | Lycoming IO-540K1G5D |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | San Diego, CA -
United States of America
|
| Phase: | Initial climb |
| Nature: | Ferry/positioning |
| Departure airport: | |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRCRAFT COLLIDED WITH THE AIRPORT PERIMETER FENCE AFTER THE PILOT EXPERIENCED A LOSS OF ENGINE POWER IMMEDIATELY AFTER TAKEOFF. THE PILOT WAS FERRYING THE AIRCRAFT WITHOUT A PERMIT TO ANOTHER AIRFIELD TO FIX A KNOWN ENGINE EXHAUST SYSTEM DISCREPANCY. A MAINTENANCE PERSON ADVISED THE PILOT BEFOREHAND THAT THE AIRCRAFT SHOULD NOT BE FLOWN WITH THE PROBLEM. THE AIRCRAFT SERVICE MANUAL INDICATES LOW ENGINE POWER COULD BE CAUSED BY A RESTRICTION IN THE EXHAUST SYSTEM. THE MUFFLER WAS FOUND TO BE BROKEN IN THE AREA ADJACENT TO THE NUMBER 6 CYLINDER STACK ATTACH POINT.
Probable Cause: THE PILOT OPERATING THE AIRCRAFT WITH A KNOWN ENGINE DISCREPANCY THAT WOULD CAUSE THE ENGINE TO LOSE POWER DUE TO RESTRICTION TO THE EXHAUST SYSTEM.
Accident investigation:
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|
| | |
| Investigating agency: | NTSB |
| Report number: | LAX91LA374 |
| Status: | Investigation completed |
| Duration: | 1 year and 8 months |
| Download report: | Final report
|
|
Sources:
NTSB LAX91LA374
Location
Revision history:
| Date/time | Contributor | Updates |
| 19-Mar-2024 17:05 |
ASN Update Bot |
Added |
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