| Date: | Monday 2 July 1990 |
| Time: | 14:45 LT |
| Type: | Cessna 337 |
| Owner/operator: | Sky Master Center |
| Registration: | N337GB |
| MSN: | 3370098 |
| Total airframe hrs: | 1400 hours |
| Engine model: | Continental IO-360 |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Bedford, NY -
United States of America
|
| Phase: | En route |
| Nature: | Ferry/positioning |
| Departure airport: | Norwood, MA (KOWD) |
| Destination airport: | Atlantic City, NJ (KAIY) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT WAS OPERATING THE AIRPLANE ON A FERRY PERMIT WHEN HE EXPERIENCED A DOUBLE POWER LOSS DUE TO FUEL STARVATION. THE PILOT DITCHED IN A RESERVOIR. NORMALLY THE LEFT TANK FEEDS THE FRONT ENGINE AND RIGHT TANK FEEDS THE REAR ENGINE. POST CRASH EXAMINATION SHOWED BOTH ENGINES WERE BEING FED FROM THE LEFT TANK, DUE TO A BENT REAR ENGINE FUEL LEVER SELECTOR CONTROL CABLE.
Probable Cause: THE FAILURE OF THE PILOT TO MONITOR THE FUEL GAUGES AND FUEL STARVATION. A FACTOR RELATED TO THE ACCIDENT WAS THE FAILURE OF MAINTENANCE PERSONNEL TO DETECT THE BENT CONDITION OF THE REAR ENGINE TANK FUEL SELECTOR CONTROL CABLE.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | NYC90LA147 |
| Status: | Investigation completed |
| Duration: | 2 years and 6 months |
| Download report: | Final report
|
|
Sources:
NTSB NYC90LA147
Location
Revision history:
| Date/time | Contributor | Updates |
| 21-Mar-2024 10:55 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation