| Date: | Friday 23 February 1990 |
| Time: | 12:00 LT |
| Type: | Cessna 170A |
| Owner/operator: | Private |
| Registration: | N9130A |
| MSN: | 18889 |
| Year of manufacture: | 1949 |
| Total airframe hrs: | 4475 hours |
| Engine model: | Continental C-145 |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Gallup, NM -
United States of America
|
| Phase: | Initial climb |
| Nature: | Unknown |
| Departure airport: | (KGUP) |
| Destination airport: | (KGUP) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRCRAFT HIT A DITCH DURING A FORCED LANDING AFTER THE ENGINE SEIZED DURING INITIAL CLIMB AFTER TAKEOFF. THIS WAS THE FIRST FLIGHT ON A NEWLY REBUILT ENGINE. THE ENGINE HAD BEEN RUN IN ON THE GROUND AND THE PILOT MADE THREE FULL POWER, STATIC RUNS BEFORE TAKEOFF. AN FAA INSPECTOR EXAMINED THE ENGINE AFTER THE ACCIDENT. HE SAID THE SPARK PLUGS FROM CYLINDERS NUMBER 1, 3, & 5 SHOWED EVIDENCE OF HAVING RUN WITH A LEAN MIXTURE. THE NUMBER 3 & 5 CYLINDERS WERE SCUFFED AND METAL FROM THE PISTONS HAD TRANSFERRED TO THE CYLINDER WALLS.
Probable Cause: IMPROPER OPERATION OF THE ENGINE DURING PREFLIGHT PREPARATION, WHICH RESULTED IN OVERHEATING OF THE ENGINE AND DAMAGE TO INTERNAL COMPONENTS.
Accident investigation:
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| | |
| Investigating agency: | NTSB |
| Report number: | DEN90LA064 |
| Status: | Investigation completed |
| Duration: | 2 years and 7 months |
| Download report: | Final report
|
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Sources:
NTSB DEN90LA064
Revision history:
| Date/time | Contributor | Updates |
| 22-Mar-2024 13:47 |
ASN Update Bot |
Added |
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