| Date: | Tuesday 7 November 1989 |
| Time: | 10:45 LT |
| Type: | Air Tractor AT-301 |
| Owner/operator: | Ellinwood Flying Service, Inc. |
| Registration: | N3158Z |
| MSN: | 301-0457 |
| Total airframe hrs: | 2365 hours |
| Engine model: | P&W R1340-AN1 |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Ellinwood, KS -
United States of America
|
| Phase: | Initial climb |
| Nature: | Agricultural |
| Departure airport: | |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT REPORTED THAT DURING CLIMBOUT HE BELIEVED THE AIRCRAFT SUSTAINED A PARTIAL LOSS OF ENG PWR. HE DUMPED HIS CHEMICAL LOAD AS THE ACFT DESCENDED. HE MANEUVERED THE ACFT TO AVOID SEVERAL OBSTACLES, BUT THE LEFT GEAR EVENTUALLY SEPARATED AFTER THE ACFT LANDED IN SOFT DIRT. A POST ACCIDENT EXAMINATION OF THE AIRCRAFT AND THE ENGINE FAILED TO ACCOUNT FOR THE REPORTED PARTIAL LOSS OF ENGINE PWR; THE DISASSEMBLY OF THE ENG DID NOT REVEAL ANY PRE-IMPACT MALFUNCTION.
Probable Cause: THE PARTIAL FAILURE OF THE ENGINE FOR UNDETERMINED REASONS WHICH RESULTED IN A FORCED LANDING. A FACTOR RELATED TO THE ACCIDENT WAS THE SOFT DIRT.
Accident investigation:
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|
| | |
| Investigating agency: | NTSB |
| Report number: | MKC90LA030 |
| Status: | Investigation completed |
| Duration: | 1 year and 10 months |
| Download report: | Final report
|
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Sources:
NTSB MKC90LA030
Location
Revision history:
| Date/time | Contributor | Updates |
| 22-Mar-2024 18:18 |
ASN Update Bot |
Added |
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