| Date: | Tuesday 10 October 1989 |
| Time: | 20:27 LT |
| Type: | Hiller UH-12E |
| Owner/operator: | West Farm Air Inc. |
| Registration: | N689SB |
| MSN: | 1475 |
| Engine model: | Lycoming VO-540 |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Yuma, AZ -
United States of America
|
| Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
| Nature: | Agricultural |
| Departure airport: | Somerton, AZ |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT COMPLETED AN AERIAL APPLICATION OPERATION AT ABOUT 200 FT AGL WHEN HE NOTICED THE ENGINE RPM DECAYING. HE PROCEEDED TO AN OPEN AREA TO EXECUTE A PRECAUTIONARY LANDING. UPON ARRIVING OVER THE OPEN AREA AT ABOUT 100 FT AGL, THE ENGINE SUSTAINED A TOTAL LOSS OF POWER. THE PLT IMMEDIATELY EXECUTED AN AUTOROTATION, BUT FLARED TOO HIGH CAUSING THE TAIL ROTOR ASSEMBLY TO STRIKE THE GROUND. A WRECKAGE EXAM DSCLSD THAT THE ENGINE TORSIONAL COUPLING RUBBER MOUNTS HAD SEPARATED. THIS CONDITION CAUSED AN OVERSPEED WHICH ULTIMATELY SHUT DOWN THE ENGINE.
Probable Cause: THE PILOT MISJUDGED THE FLARE ALTITUDE. CONTRIBUTING TO THIS ACCIDENT WAS THE FAILURE OF THE ENGINE TORSIONAL COUPLING WHICH ULTIMATELY CAUSED THE TOTAL LOSS OF POWER.
Accident investigation:
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| | |
| Investigating agency: | NTSB |
| Report number: | LAX90DUJ03 |
| Status: | Investigation completed |
| Duration: | 2 years and 9 months |
| Download report: | Final report
|
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Sources:
NTSB LAX90DUJ03
Location
Revision history:
| Date/time | Contributor | Updates |
| 22-Mar-2024 19:38 |
ASN Update Bot |
Added |
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