| Date: | Monday 25 September 1989 |
| Time: | 21:30 LT |
| Type: | Cessna 177RG |
| Owner/operator: | Russell Wisler |
| Registration: | N52665 |
| MSN: | 1238 |
| Engine model: | Lycoming IO360A1B6D |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Tucson, AZ -
United States of America
|
| Phase: | Approach |
| Nature: | Unknown |
| Departure airport: | Phoenix, AZ (KPHX) |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT REPORTED THAT DURING A NIGHT VISUAL APPROACH, ABOUT 4-5 MI FROM THE AIRPORT, THE ENGINE LOST POWER. A FORCED LANDING WAS MADE IN A FIELD AND THE AIRCRAFT COLLIDED WITH A TELEPHONE POLE. NO PRE-IMPACT RELATED MALFUNCTIONS WERE FOUND IN THE ENGINE, AND THE ENGINE RAN SUCCESSFULLY AFTER THE ACCIDENT. THE PILOT LATER STATED THAT THE ENGINE HAD CONTINUED TO OPERATE THROUGHOUT THE APPROACH AND LANDING. THE PILOT HAD 5 HRS IN MAKE/MODEL.
Probable Cause: A LOSS OF ENGINE POWER DUE TO THE PILOT'S IMPROPER USE OF THE AIRCRAFT'S POWERPLANT CONTROLS. A CONTRIBUTING FACTOR WAS THE PILOT'S LIMITED EXPERIENCE IN A CESSNA 177RG.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | LAX89LA323 |
| Status: | Investigation completed |
| Duration: | 2 years and 9 months |
| Download report: | Final report
|
|
Sources:
NTSB LAX89LA323
Location
Revision history:
| Date/time | Contributor | Updates |
| 22-Mar-2024 20:37 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation