| Date: | Sunday 15 November 1987 |
| Time: | 12:27 |
| Type: | Mooney M20C |
| Owner/operator: | Renato & Glenda Ricci |
| Registration: | N6670R |
| MSN: | 2865 |
| Year of manufacture: | 1964 |
| Total airframe hrs: | 2433 hours |
| Engine model: | Lycoming O-360-A1D |
| Fatalities: | Fatalities: 4 / Occupants: 4 |
| Other fatalities: | 0 |
| Aircraft damage: | Destroyed |
| Category: | Accident |
| Location: | Grand Canyon, AZ -
United States of America
|
| Phase: | Approach |
| Nature: | Private |
| Departure airport: | Sedona, AZ (SEZ) |
| Destination airport: | Death Valley, CA (L06) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WHILE CRUISING EN ROUTE ALL ENGINE POWER WAS SUDDENLY LOST AND THE PLT ATTEMPTED AN EMERGENCY LDG AT THE GRAND CANYON ARPT. DURING THE GLIDE, THE ACFT CRASHED INTO AN OUTCROP OF ROCKS ON A STEEP CLIFF, 0.5 MI FROM THE END OF THE RWY. EXAM OF THE ENGINE REVEALED THAT ONE OF THE #3 CONNECTING ROD BOLT NUTS HAD BACKED OFF THE BOLT, AND OTHER NUT HAD BEEN PARTIALLY STRIPPED OFF ITS BOLT. THE ENGINE HAD BEEN OPERATED FOR 212 HRS SMOH. LAB EXAM OF THE BOLT/NUT INTERFACE INDICATED THAT THE NUTS HAD BEEN UNDERTORQUED WHEN THEY WERE LAST INSTALLED. CAUSE:
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | LAX88FA042 |
| Status: | Investigation completed |
| Duration: | |
| Download report: | Final report
|
|
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001213X32541 Revision history:
| Date/time | Contributor | Updates |
| 24-Oct-2008 10:30 |
ASN archive |
Added |
| 21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency, ] |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation