| Date: | Monday 17 April 1989 |
| Time: | 13:05 LT |
| Type: | Bell UH-1E |
| Owner/operator: | Helicopter Systems |
| Registration: | N118HS |
| MSN: | 155341 |
| Year of manufacture: | 1968 |
| Total airframe hrs: | 5414 hours |
| Engine model: | Lycoming T-53-L-11D |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Aiken, SC -
United States of America
|
| Phase: | En route |
| Nature: | Unknown |
| Departure airport: | |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE HELICOPTER WAS BEING OPERD AT APRX 100 FT AGL WITH A HOPPER EXTDD FROM A CABLE. WITNESSES HEARD A LOUD POPPING SOUND. AS THEY LOOKED IN THE DRCTN OF THE HELICOPTER, THEY NOTED THE TAIL ROTOR WAS NOT TURNING & ONE BLADE APPEARED TO BE HANGING. THE PLT RPRTD THERE WAS NO WARNING OF AN IMPENDING ANTI-TORQUE CONTROL PROBLEM WHEN HE LOST CONTROL OF THE HELICOPTER. THE HELICOPTER THEN COLLIDED WITH TREES & CRASHED. INV REVEALED THE PLT HAD RPRTD AN OIL LEAK FM THE 90 DEG GEARBOX ON 4/11/89. THE COMPANY MECHANIC SUBSEQUENTLY REPLACED THE GEARBOX & A FUNCTIONAL TEST FLT WAS COMPLETED. THE ACDNT OCCURRED AFTER APRX ANOTHER 6 HRS OF OPN. AN EXAM OF THE TAIL ROTOR ASSEMBLY REVEALED THAT 1 OF THE 2 RETENTION BOLTS WERE MISSING FM THE TAIL ROTOR PITCH CHANGE CROSSHEAD. THREADED IMPRINTS WERE FND INSIDE THE RESPECTIVE CROSSHEAD RETENTION THRU-BOLT HOLE. THE RETENTION BOLT, NUT, WASHER & COTTER PIN WERE NOT RECOVERED. BOTH TAIL ROTOR BLADES CONTAINED CHORDWISE MARKS WHICH CORRESPONDED TO MARKS ON THE VERTICAL FIN (OPPOSITE OF THE TAIL ROTOR TIP PATH PLANE).
Probable Cause: IMPROPER INSTALLATION OF A TAIL ROTOR PITCH CHANGE CROSSHEAD RETENTION BOLT BY THE COMPANY MECHANIC, WHICH RESULTED IN LOOSENING OF THE BOLT AND EVENTUAL FAILURE OF THE TAIL ROTOR ASSEMBLY/BLADE AND SUBSEQUENT LOSS OF CONTROL. TREES AT THE CRASH SITE CONTRIBUTED TO HELICOPTER DAMAGE.
Accident investigation:
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| | |
| Investigating agency: | NTSB |
| Report number: | ATL89FA130 |
| Status: | Investigation completed |
| Duration: | 1 year and 4 months |
| Download report: | Final report
|
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Sources:
NTSB ATL89FA130
Location
Revision history:
| Date/time | Contributor | Updates |
| 24-Mar-2024 08:49 |
ASN Update Bot |
Added |
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