| Date: | Tuesday 6 September 1988 |
| Time: | 13:22 LT |
| Type: | Piper PA-24-260 |
| Owner/operator: | Private |
| Registration: | N8670P |
| MSN: | 24-4118 |
| Year of manufacture: | 1965 |
| Total airframe hrs: | 2385 hours |
| Engine model: | Lycoming IO-540-D4A5 |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Punta Gorda, FL -
United States of America
|
| Phase: | Approach |
| Nature: | Private |
| Departure airport: | Gainesville, GA (KGVL) |
| Destination airport: | Ft. Myers, FL (KFMY) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT WAS RETURNING FROM VFR XC FLT DURING WHICH MANY CLIMBS, DESCENTS & DETOURS WERE MADE TO AVOID ADVERSE WX & MAINTAIN VFR. HE STATED THE STRONG HEADWINDS CONSIDERABLY REDUCED HIS GRNDSPEED. AT HIS 1ST INTENDED LDG ARPT, STRONG GUSTY X-WINDS MADE THE APRCH 'SQUIRRELLY' & HE ABANDONED THE ATTEMPT & FLEW TO AN ARPT WITH WIDER RWYS NEARLY ALIGNED WITH THE WIND. AT ABOUT 800 FT TURNING BASE TO FINAL, THE ENG QUIT DUE TO FUEL STARVATION & THE PLT WAS TOO LOW TO REGAIN ENG POWER. A FORCED LDG WAS ATTEMPTED ON A ROAD, BUT THE ACFT CLIPPED A POWERLINE WHICH THREW THE ACFT OUT OF CONTROL & IT CRASHED INTO A DITCH. THE PLT LATER STATED TO AVOID AN ACCIDENT SUCH AS THIS IN THE FUTURE, HE WOULD PAY MORE POSITIVE ATTENTION TO FUEL CONSUMPTION & QUANTITY OF FUEL REMAINING IN EACH TANK.
Probable Cause:
Accident investigation:
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|
| | |
| Investigating agency: | NTSB |
| Report number: | MIA88LA266 |
| Status: | Investigation completed |
| Duration: | 1 year |
| Download report: | Final report
|
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Sources:
NTSB MIA88LA266
Location
Revision history:
| Date/time | Contributor | Updates |
| 24-Mar-2024 18:57 |
ASN Update Bot |
Added |
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