| Date: | Saturday 3 September 1988 |
| Time: | 12:15 LT |
| Type: | Cessna 177RG |
| Owner/operator: | Michael Oil Company, Inc. |
| Registration: | N52655 |
| MSN: | 177RG1232 |
| Year of manufacture: | 1977 |
| Total airframe hrs: | 3068 hours |
| Engine model: | Lycoming IO-360-A1B6 |
| Fatalities: | Fatalities: 0 / Occupants: 4 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Berkeley, KY -
United States of America
|
| Phase: | En route |
| Nature: | Private |
| Departure airport: | Springfield, MO |
| Destination airport: | Hopkinsville, KY |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT REPORTED THAT HE DEPARTED WITH 6 HRS OF FUEL ON BOARD. HE ENCOUNTERED LOW CEILINGS WHILE EN ROUTE, AND FLEW AT 3-500 FT AGL TO MAINTAIN VFR. ABOUT 3 HRS & 15 MINUTES AFTER DEPARTURE, THE ENGINE SPUTTERED AND LOST POWER. THE PLT MADE A FORCED LDG IN TREES. WHILE SECURING THE AIRPLANE, HE OBSERVED THE FUEL SELECTOR IN THE 'LEFT' (TANK) POSITION INSTEAD OF IN THE 'BOTH' POSITION WHERE HE NORMALLY POSITIONED IT FOR FLIGHT. POST-CRASH EXAM OF THE AIRPLANE AT THE SITE BY AN IA MECHANIC REVEALED THAT THE RIGHT TANK WAS COMPLETELY FULL OF FUEL. THE LEFT TANK WAS IMPACT DAMAGED & CONTAINED ONLY ABOUT A PINT OF FUEL. THE PLT NOTED THAT THE AIRPLANE FUEL GAUGES WERE NOT OPERATIONAL, AND THAT HE KEPT TRACK OF FUEL CONSUMPTION BY ELAPSED TIME AND KNOWN AVERAGE FUEL FLOW PER HOUR.
Probable Cause:
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | ATL88LA244 |
| Status: | Investigation completed |
| Duration: | 1 year and 3 months |
| Download report: | Final report
|
|
Sources:
NTSB ATL88LA244
Location
Revision history:
| Date/time | Contributor | Updates |
| 24-Mar-2024 19:16 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation