| Date: | Wednesday 19 March 1986 |
| Time: | 17:25 |
| Type: | Thorp T-18 |
| Owner/operator: | private |
| Registration: | N83GD |
| MSN: | 832 |
| Engine model: | Lycoming O-320-E2A |
| Fatalities: | Fatalities: 2 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Lakeland, FL -
United States of America
|
| Phase: | En route |
| Nature: | Private |
| Departure airport: | |
| Destination airport: | Hollywood, FL (HWO) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WITNESSES OBSERVED BLACK SMOKE TRAILING FROM THE HOMEBUILT ACFT DURING TAKEOFF & INITIAL CLIMB. THE ACFT WAS OBSERVED TO CLIMB TO AN ESTIMATED ALT OF 150 TO 200 FT WHERE ENG SOUND CEASED & THE PROP STOPPED. THE ACFT WAS THEN OBSERVED TO ATTEMPT A LEFT TURN BACK TOWARD THE RWY. DURING THE TURN, THE NOSE CAME UP & WITNESSES STATED THAT THE ACFT STALLED ABOUT ONE-HALF WAY THROUGH THE TURN & CRASHED TO THE GROUND. AN EXAM OF THE COCKPIT REVEALED THAT THE HAND ACTUATED FUEL PRIMER WAS IN THE UNLOCKED & OUT POSITION. A REVIEW OF THE ACFT'S CHECKLISTS FAILED TO REVEAL ANY REFERENCE TO ENSURING THAT THE PRIMER IS IN & LOCKED AFTER ENGINE START. CAUSE:
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | MIA86FA101 |
| Status: | Investigation completed |
| Duration: | |
| Download report: | Final report
|
|
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001213X33122 Revision history:
| Date/time | Contributor | Updates |
| 24-Oct-2008 10:30 |
ASN archive |
Added |
| 21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency, ] |
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