| Date: | Tuesday 2 August 1988 |
| Time: | 00:15 LT |
| Type: | Varga 2150A |
| Owner/operator: | Private |
| Registration: | N8259J |
| MSN: | VAC-105-78 |
| Engine model: | Lycoming O-320-A |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Washington, IA -
United States of America
|
| Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
| Nature: | Private |
| Departure airport: | Oshkosh, WI |
| Destination airport: | Memphis, MI |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WHILE ENROUTE THE PIC RPTD A LOSS OF ENG PWR. THE PIC STATED IN HIS RPT THAT HAVING PASSED WASHINGTON, IA, HE SWITCHED FUEL TANKS TO DRAW FUEL FROM THE LFT TANK WHICH INDICATED 1/2 FULL. SHORTLY AFTER SWITCHING, THE PIC STATED THE TANK WENT EMPTY. THE PIC THEN SWITCHED ON THE OTHER TANK WHICH HAD INDICATED 1/4 FULL. SHORTLY AFTER DOING SO, THE ENG QUIT AND THE PIC ATTEMPTED TO GLIDE TO THE WASHINGTON, IA, ARPT. THE ACFT CLIPPED A POWERLINE GUY WIRE DURING THE FORCED LANDING AND CRASHED SHORT INTO A FARM IMPLEMENT SALES LOT. INSP OF THE ACFT REVEALED LESS THAN 1 GAL TOTAL FUEL QUANTITY. NO LEAKS OR RUPTURE OF FUEL SYSTEM HARDWARE WAS FOUND WHICH COULD EXPLAIN THE LOW QUANTITY OF FUEL IN THE SYSTEM.
Probable Cause:
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | MKC88LA146 |
| Status: | Investigation completed |
| Duration: | 1 year and 2 months |
| Download report: | Final report
|
|
Sources:
NTSB MKC88LA146
Location
Revision history:
| Date/time | Contributor | Updates |
| 25-Mar-2024 07:13 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation