ASN Wikibase Occurrence # 37077
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Date: | Sunday 10 September 1989 |
Time: | 15:18 |
Type: | Aero Commander 680FLP |
Owner/operator: | private |
Registration: | N22LR |
MSN: | 1503-18 |
Year of manufacture: | 1965 |
Total airframe hrs: | 4790 hours |
Fatalities: | Fatalities: 1 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Kailua-Kona, Hawaii, HI -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | (KOA) |
Destination airport: | Honolulu, HI (HNL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:AS THE ACFT WAS DEPG FM RWY 17, SMOKE WAS OBSERVED COMING FM THE RGT ENG. THE PLT CONFIRMED A LOSS OF PWR & MADE A RGT TURN BACK TOWARD THE RWY, THEN RPRTD HE HAD 'LOST BOTH ENGINES.' THE ACFT WAS EXTENSIVELY DMGD DURING A LNDG ON ROUGH, ROCKY TRRN ABT 1/4 MI SW OF THE RWY THRESHOLD. INVESTIGATION REVEALED THE ACFT HAD JUST CHANGED OWNERSHIP. DURING PRE- PURCHASE INSPN IN FLORIDA, METAL PARTICLES WERE FND IN THE OIL SCREENS OF BOTH ENGS. OIL WAS CHGD & FLUSHED, BUT METAL PARTICLES WERE FND AFTER ANOTHER ENG RUN. IN MAY 1989, THE RGT ENG WAS REPLACED WITH AN ENG FM ANOTHER ACFT. THE ACFT WAS FLOWN TO OAKLAND, CA, WHERE IT WAS PAINTED & NEW INTERIOR WAS INSTALLED. A LCL MECH NOTED METAL PARTICLES IN BOTH ENG OIL SCREENS & RCMNDD OIL ANALYSIS, BUT FERRYING PLT REFUSED. AFTER FLT TO HAWAII, NO OIL STAIN NOTED ON FUSELAGE BFRFLT ON 9/9/89. EXAM OF WRECKAGE REVEALED BOTH ENGS FAILED FM DETONATION. HVY OIL STREAKS FND BHND RGT ENG, SOME STREAKS OF OIL FND BHND LEFT ENG. RGT ENG CRANKSHAFT/ROD BRG SURFACE WAS 0.010' UNDER STANDARD, BUT ROD BRGS WERE STANDARD SIZE. CAUSE: INADEQUATE MAINTENANCE, AND OPERATION BY THE PILOT WITH KNOWN DEFICIENCIES IN THE AIRCRAFT. FACTORS RELATED TO THE ACCIDENT WERE: EXCESSIVE WEAR IN BOTH ENGINES, IMPROPER USE OF POWERPLANT CONTROLS BY THE PILOT, SUBSEQUENT OVERTEMPERATURE/DETONATION IN BOTH ENGINES, IMPROPER EMERGENCY PROCEDURES BY THE PILOT (INCLUDING PREMATURE GEAR EXTENSION AND/OR FAILURE TO PROPERLY REDUCE DRAG ON THE AIRCRAFT AFTER LOSS OF ENGINE POWER), AND THE PILOT'S LACK OF EXPERIENCE IN MULTI-ENGINE AND THIS MAKE AND MODEL OF AIRCRAFT.
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001213X29401 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Jun-2023 08:50 |
Ron Averes |
Updated [[Time, Damage, Category, Investigating agency]] |
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