| Date: | Wednesday 9 December 1987 |
| Time: | 11:45 LT |
| Type: | Beechcraft B24R |
| Owner/operator: | Private |
| Registration: | N1999L |
| MSN: | MC-432 |
| Total airframe hrs: | 1826 hours |
| Engine model: | Lycoming IO-360-A1B6 |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Sewanee, TN -
United States of America
|
| Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
| Nature: | Private |
| Departure airport: | Mckenny, TX |
| Destination airport: | Fayetteville, NC (KFAY) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT RPRTD THAT HE OBTAINED A WX BRIEFING BEFORE TAKEOFF & THAT THE WX AT HIS INTENDED DESTINATION WAS RPRTD AS MARGINAL. WHILE EN ROUTE, HE ENCOUNTERED WX AND CLIMBED ABOVE IT. APRX 4 HRS AFTER DEPARTURE, HE BECAME CONCERNED ABOUT THE REMAINING FUEL SUPPLY AND ELECTED TO LAND. HE FOUND AN OPENING IN THE CLOUD COVER AND BEGAN A DESCENT. AS THE ACFT DESCENDED, THE PLT BECAME AWARE THAT HE WAS NEAR A MTN TOP. HE STATED THE ACFT ENCOUNTERED WIND CURRENTS AND BECAME DIFFICULT TO CONTROL; AND SUBSEQUENTLY, THE WINDS FORCED IT DOWN INTO THE TREES. A NEARBY HUNTER, WHO HEARD THE CRASH, SAID THE WX WAS FOGGY AND LIGHT DRIZZLE WAS FALLING.
Probable Cause:
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | ATL88LA054 |
| Status: | Investigation completed |
| Duration: | 1 year and 3 months |
| Download report: | Final report
|
|
Sources:
NTSB ATL88LA054
Location
Revision history:
| Date/time | Contributor | Updates |
| 26-Mar-2024 09:33 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation