| Date: | Tuesday 16 June 1987 |
| Time: | 15:42 LT |
| Type: | Beechcraft 3NM |
| Owner/operator: | Rhoades Aviation |
| Registration: | N37CB |
| MSN: | CA235 |
| Total airframe hrs: | 9486 hours |
| Engine model: | P&W R-985 |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Cahokia, IL -
United States of America
|
| Phase: | Initial climb |
| Nature: | Ferry/positioning |
| Departure airport: | Cahokia, IL (KCPS) |
| Destination airport: | Seymour, IN (KSER) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE ACFT EXPERIENCED A LOSS OF PWR IN THE RT ENG IMMEDIATELY AFT TKOF. THE PLT WAS NOT ABLE TO FEATHER THE PROPELLER AND WAS FORCED TO LAND IN A WHEAT FIELD ON ARPT PROPERTY. CONDITIONS WERE CONDUCIVE TO CARBURETOR ICING AT THE TIME OF THE ACCD. INVESTIGATION REVEALED THAT THE RT PROPELLER HUB WAS IMPROPERLY ASSEMBLED AND WOULD NOT ALLOW THE PROPELLER TO FEATHER. IN ADDITION, THE RT CARBURETOR HEAT SYSTEM WAS INOPERATIVE BECAUSE THE DUCTS THAT CONNECT THE MANIFOLD HEAT MUFFS TO THE CARBURETOR AIR BOX WERE MISSING.
Probable Cause:
Accident investigation:
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| | |
| Investigating agency: | NTSB |
| Report number: | CHI87DCA01 |
| Status: | Investigation completed |
| Duration: | 1 year and 5 months |
| Download report: | Final report
|
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Sources:
NTSB CHI87DCA01
Location
Revision history:
| Date/time | Contributor | Updates |
| 27-Mar-2024 07:02 |
ASN Update Bot |
Added |
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