| Date: | Tuesday 9 June 1987 |
| Time: | 17:30 LT |
| Type: | Piper PA-28R-201 |
| Owner/operator: | Beaver Aviation Service, Inc. |
| Registration: | N3965M |
| MSN: | 28R7837145 |
| Total airframe hrs: | 5259 hours |
| Engine model: | Lycoming IO-360-C1C6 |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Unity, OH -
United States of America
|
| Phase: | Landing |
| Nature: | Training |
| Departure airport: | Beaver Falls, PA (KBVI) |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE CFI REPORTED THAT HE REDUCED PWR TO NEAR IDLE WITH THE THROTTLE, TO HAVE HIS STUDENT PRACTICE A SIMULATED FORCED LDG. THE ENGINE SUBSEQUENTLY LOST PWR COMPLETELY AT ABOUT 400-500 FT AGL WHEN HE ATTEMPTED TO ADD PWR BACK SO THAT THE STUDENT COULD INITIATE A GO-AROUND. SUBSEQUENT EFFORTS TO REGAIN PWR WERE UNSUCCESSFUL, AND A FORCED LDG WAS MADE IN A FIELD. THE CFI NOTED THAT HE HAD INCREASED THE PWR MOMENTARILY SEVERAL TIMES DURING DESCENT TO 'CLEAR' THE ENGINE, AND THAT HE WAS 'SLOWLY' OPENING THE THROTTLE WHEN THE ENGINE LOST PWR. POST-ACCIDENT EXAMINATION OF THE AIRPLANE AND ENGINE BY THE FAA REVEALED NO EVIDENCE OF ANY PRE-EXISTING MALFUNCTION OR FAILURE.
Probable Cause:
Accident investigation:
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|
| | |
| Investigating agency: | NTSB |
| Report number: | ATL87LA164 |
| Status: | Investigation completed |
| Duration: | 1 year and 2 months |
| Download report: | Final report
|
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Sources:
NTSB ATL87LA164
Location
Revision history:
| Date/time | Contributor | Updates |
| 27-Mar-2024 07:28 |
ASN Update Bot |
Added |
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