| Date: | Wednesday 28 January 1987 |
| Time: | 01:43 LT |
| Type: | Cessna 402B |
| Owner/operator: | Benjamin Gilbert |
| Registration: | N69310 |
| MSN: | 402B0428 |
| Year of manufacture: | 1973 |
| Total airframe hrs: | 6897 hours |
| Engine model: | Continental TSIO-520-E |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Las Vegas, NV -
United States of America
|
| Phase: | Approach |
| Nature: | Unknown |
| Departure airport: | Albuquerque, NM |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:PLT FILED IFR, 2 40 ETE. DUE DELAY, PLT DEPARTED VFR AND OPENED VFR FLT PLAN. ENROUTE, STONG HDWINDS ENCOUNTERED. ALSO, CLOUDS REQUIRED ALTITUDE AND COURSE DEVIATIONS TO MAINTAIN VFR. ATE WAS 3 33. ON FINAL, LEFT ENG LOST PWR, RT ENG BEGAN SURGING. INTO 20-KT HDWIND, ACFT LANDED HARD SHORT OF RWY, COLLAPSING GEAR. INVESTIGATION SHOWED FUEL STARVATION. ALL FUEL GAGES ERRONEOUS; MAINS SHOWED 50 AND 100 LBS REMAINING AFTER DRAINING RESIDUAL 1-2 GALS. AUX TANKS WERE NEAR FULL, 20-GAL LOCKER TANK WAS FULL. PLT STATED FLIGHT CONDUCTED ON MAIN TANKS EXCEPT AUX TANKS USED FOR 30-40 MINS ENROUTE. WT & BAL RECORD SHOWED 100 GALS FUEL, BUT PLT HAD ORDERED TOP-OFF (180 GALS).
Probable Cause:
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | SEA87LA049 |
| Status: | Investigation completed |
| Duration: | 1 year and 2 months |
| Download report: | Final report
|
|
Sources:
NTSB SEA87LA049
Location
Revision history:
| Date/time | Contributor | Updates |
| 27-Mar-2024 15:29 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation