| Date: | Monday 7 October 1985 |
| Time: | 17:42 LT |
| Type: | Fairchild F-27 |
| Owner/operator: | Private |
| Registration: | N4302F |
| MSN: | 60 |
| Engine model: | ROLLS-ROYCE 514-7 |
| Fatalities: | Fatalities: 0 / Occupants: 3 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Houston, TX -
United States of America
|
| Phase: | Landing |
| Nature: | Ferry/positioning |
| Departure airport: | Tampas, FL (KTPA) |
| Destination airport: | Houston, TX (KHOU) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:ACFT VEERED LEFT OFF THE RUNWAY SHORTLY AFTER TOUCHDOWN, COLLAPSING THE NOSE GEAR. WINDS AT THE TIME WOULD HAVE RESULTED IN DIRECT CROSSWIND OF 9 KNS. THE CREW THAT WAS CONTRACTED TO FERRY THE ACFT NOTED, WHEN THEY PICKED IT UP, THAT THERE WERE SEVERAL OPEN EQUIPMENT DISCREPANCIES, INCLUDING ONE THAT STATED THAT THE PRIMARY PROP GROUND FINE PITCH CONTROL SYS WAS INOP. PRIOR TO THE ACCIDENT LNDG, THE CREW HAD MADE 2 LANDINGS USING THE SECONDARY SYS, WHICH INVOLVED ENGAGING THE GUST LOCK ON, MOMENTARILY AFTER TOUCHDOWN, TO ENGAGE THE PROP CONTROLS. THE PIC STATED THAT THIS PROCEDURE WAS DONE AFTER TOUCHDOWN AND THAT AT THE SAME TIME HE NOTICED THE ACFT VEERING LEFT. HE COULD NOT CORRECT WITH EITHER RUDDER OR NOSE GEAR STEERING.
Probable Cause:
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | FTW86LA006 |
| Status: | Investigation completed |
| Duration: | |
| Download report: | Final report
|
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Sources:
NTSB FTW86LA006
Location
Revision history:
| Date/time | Contributor | Updates |
| 29-Mar-2024 12:48 |
ASN Update Bot |
Added |
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