ASN Wikibase Occurrence # 37658
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Date: | Thursday 5 September 1996 |
Time: | 02:27 LT |
Type: | Beechcraft D55 Baron |
Owner/operator: | Gta Investments Inc. |
Registration: | N873LB |
MSN: | TE-711 |
Year of manufacture: | 1969 |
Total airframe hrs: | 9196 hours |
Engine model: | Continental IO-520-C |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Corsicana, TX -
United States of America
|
Phase: | En route |
Nature: | Unknown |
Departure airport: | Houston, TX (KHOU) |
Destination airport: | Dallas, TX (KDAL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was on a night cross-country freight flight. A pilot witness reported that the pilot told him, on 122.85, that his left engine had failed. A second pilot witness reported hearing the pilot transmit that the engine came back on line when he switched to the aux tank, but he decided to make a precautionary landing prior to Dallas anyway. The pilot transmitted to ATC: 'I will contact you when I get on the ground and let you know the name of the airport.' The airport had pilot controlled lighting, on 122.80, which included a VASI approach system. The airplane was found with the gear down, the flaps down, the left propeller at low pitch but not feathered, and the right engine throttle at idle. The fuel selectors were found with the right one on the main tank and the left one on the aux tank. No fuel was found in the left wing tanks. The second pilot witness stated that she flew the airplane the night before, and that fuel had siphoned from the left main tank, which she reported to dispatch upon landing. Postcrash examination of the left wing main fuel port collar revealed deformations in the collar. The pilot had completed his Part 135 check ride 3 days before the accident.
Probable Cause: The pilot's failure to maintain minimum control airspeed which resulted in the loss of control. Factors were the bent collar of the left main fuel tank refueling neck which resulted in fuel siphoning from the tank in flight, the pilot's failure to follow procedures to cross feed fuel from the right main tank to the left engine which led to left engine power loss by fuel starvation, the pilot's lack of total experience in the make and model of airplane, and the dark night light condition.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW96FA373 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB FTW96FA373
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-May-2022 06:28 |
PolandMoment |
Updated [Narrative] |
08-Apr-2024 19:07 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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