| Date: | Monday 6 May 1985 |
| Time: | 19:29 LT |
| Type: | Cessna 310G |
| Owner/operator: | Private |
| Registration: | N2903R |
| MSN: | 310G0103 |
| Total airframe hrs: | 3185 hours |
| Engine model: | Continental IO-470-D |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Palm City, FL -
United States of America
|
| Phase: | Initial climb |
| Nature: | Private |
| Departure airport: | |
| Destination airport: | Ft.lauderdale, FL (FXE |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PLT REPORTED THAT SHORTLY AFTER TAKEOFF, THE LEFT ENG LOST POWER. HE WAS UNABLE TO MAINTAIN CONTROL OF THE ACFT, SO HE REDUCED POWER ON THE RIGHT ENG & SUBSEQUENTLY MADE AN EMERGENCY LANDING IN A FIELD. DURING THE LANDING, THE GEAR COLLAPSED, THEN THE ACFT SLID INTO A TREE. AN INVESTIGATION REVEALED THE ACFT HAD BEEN PARKED FOR 8 MONTHS & HAD RECENTLY FLOWN FOR ONLY ABOUT 2 HRS. A POST CRASH EXAM OF THE ACFT REVEALED NO EVIDENCE OF A PREIMPACT PART FAILURE OR MALFUNCTION & A TEST RUN OF THE ENG SHOWED NO SIGNS OF A FAILURE. THE PASSENGER STATED THE LEFT FUEL FLOW METER STARTED FLUCTUATING AT THE SAME TIME THE ENG LOST P0WER, THEN THE FUEL FLOW INDICATION DROPPED TO ZERO.
Probable Cause:
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | MIA85LA165 |
| Status: | Investigation completed |
| Duration: | |
| Download report: | Final report
|
|
Sources:
NTSB MIA85LA165
Revision history:
| Date/time | Contributor | Updates |
| 30-Mar-2024 09:51 |
ASN Update Bot |
Added |
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