Accident Mooney M20K N5788U,
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ASN Wikibase Occurrence # 37799
 
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Date:Monday 29 November 1993
Time:19:49 LT
Type:Silhouette image of generic M20T model; specific model in this crash may look slightly different    
Mooney M20K
Owner/operator:Baldwin, Gerald E.
Registration: N5788U
MSN: 25-0852
Year of manufacture:1984
Engine model:CONTINENTAL TSIO-360-GB
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:June Lake, CA -   United States of America
Phase: En route
Nature:Private
Departure airport:Carson City, NV (O04)
Destination airport:Chino, CA (KCNO)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE PILOT DEPARTED ON A 329 NAUTICAL MILE CROSS-COUNTRY FLIGHT OVER MOUNTAINS AND DID NOT FILE A FLIGHT PLAN. ABOUT 88 MILES FROM THE DEPARTURE POINT, THE AIRPLANE CRASHED, BUT WAS MISSING FOR ABOUT EIGHT MONTHS. IT WAS FOUND AT ABOUT THE 12,200 FOOT LEVEL OF A MOUNTAIN, ABOUT 2 MILES WEST OF THE DIRECT COURSE LINE FROM THE DEPARTURE POINT TO THE DESTINATION. AN INVESTIGATION REVEALED EVIDENCE OF AN IN-FLIGHT BREAKUP. WRECKAGE DEBRIS WAS FOUND OVER A 1,500 FOOT AREA. THE EMPENNAGE HAD SEPARATED FROM THE FUSELAGE, BUT WAS NOT FOUND, EXCEPT THE RUDDER AND ELEVATOR COUNTERWEIGHTS WERE FOUND IN DEBRIS NORTH OF THE FUSELAGE. THE AIRPLANE WAS EQUIPPED WITH AN AREA NAVIGATION SYSTEM, LORAN-C, AND A PORTABLE GPS. THE AUTOPILOT WAS FOUND ENGAGED. EXAMINATION OF THE WRECKAGE REVEAL THAT A PITCH TRIM SPRING IN THE AUTOPILOT PITCH SERVO HAD FAILED DUE TO FATIGUE. FURTHER EXAMINATION REVEALED THE AVIONICS IN THE AIRPLANE BELONGED TO AN AIRPLANE THAT HAD BEEN REPORTED STOLEN. THERE WERE NO RECORDS FOUND OF ANY INSPECTIONS OR MAINTENANCE BEING PERFORMED ON THE ACCIDENT AIRPLANE.

Probable Cause: THE PILOT ALLOWED THE AIRPLANE TO EXCEED ITS DESIGN LIMITS (AIRSPEED AND/OR STRESS LIMITS) AFTER INADVERTENTLY ENTERING A DESCENT. FACTORS RELATING TO THE ACCIDENT WERE: DARKNESS (NIGHT OR LATE DUSK), THE PILOT'S FAILURE TO ASSURE ADEQUATE MAINTENANCE/INSPECTION OF THE AIRPLANE, AND FATIGUE FAILURE OF A PITCH TRIM SPRING IN THE AUTOPILOT PITCH SERVO.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX94FA278
Status: Investigation completed
Duration: 2 years and 2 months
Download report: Final report

Sources:

NTSB LAX94FA278

History of this aircraft

Other occurrences involving this aircraft
15 September 1985 N5788U Nicholas Mendoza 0 Rosamond, CA sub

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
12-Jan-2019 10:50 BEAVERSPOTTER Updated [Cn]
10-Apr-2024 09:53 ASN Update Bot Updated [Time, Operator, Other fatalities, Destination airport, Source, Narrative, Category, Accident report]

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