ASN Wikibase Occurrence # 37824
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Date: | Friday 15 January 1993 |
Time: | 13:43 |
Type: | Cessna 414 |
Owner/operator: | Plane Wrap |
Registration: | N4733G |
MSN: | 414-0928 |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Reno, NV -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | (RNO) |
Destination airport: | Camarillo, CA (CMA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A CESSNA 414 COLLIDED WITH A LEVEL GROUND WHILE ATTEMPTING TO LAND DURING A SNOW SHOWER. THE PILOT REPORTED AN EMERGENCY ONE MINUTE AFTER DEPARTING IFR AND REQUESTED TO RETURN TO THE AIRPORT UNDER VISUAL RULES. THE PILOT INDICATED TO AIR TRAFFIC CONTROL THAT 'I CAN'T GET ANY SPEED.' THE VISIBILITY WAS VARIABLE AROUND THE AIRPORT WITH THE LOWEST REPORT OF 1/2 MILE. WITNESSES OBSERVED THE AIRPLANE TRAVELING FAST AT LOW ALTITUDE AND INDICATED BOTH ENGINES WERE RUNNING. INVESTIGATION REVEALED DURING SERVICING BEFORE THE FLIGHT, THE PITOT TUBE COVERS WERE NOT USED. ABOUT 1.5 INCHES OF SNOW HAD ACCUMULATED ON THE AIRPLANE DURING THE REFUELING AND WAS BRUSHED OFF. THE AIRPLANE WAS SEEN FLYING INTO A SNOW SHOWER AND REVERSING COURSE. WITNESSES REPORTED THE AIRPLANE'S ANGLE OF BANK TO BE 80 TO 90 DEGREES WITH A 20 DEGREE PITCH DOWN ATTITUDE. THE AIRPLANE DESCENDED INTO A SNOW COVERED PASTURE. WITNESSES REPORTED THE AIRPLANE LEVELED ITS WING JUST BEFORE IMPACT. MANUFACTURER'S SAFETY AND WARNING SUPPLEMENTS INDICATE INFLIGHT ICE PROTECTION IS NOT DESIGNED TO REMOVE SNOW ON PARKED AIRCRAFT. THE MANUFACTURER RECOMMENDS USE OF HEATED HANGARS OR APPROVED DEICING SOLUTIONS TO INSURE THE ARE NO INTERNAL ACCUMULATIONS IN PITOT STATIC SYSTEM PORTS. CAUSE: THE FAILURE OF THE PILOT TO USE PITOT STATIC SYSTEM COVERS DURING ICING CONDITIONS WHICH RESULTED IN A BLOCKED PITOT TUBE AND SUBSEQUENT LOSS OF AIRSPEED INDICATIONS. THIS LED TO PILOT DISORIENTATION AND AN INVERTANT STALL. FACTORS TO THE ACCIDENT WERE IMPROPER SNOW REMOVAL AND ADVERSE WEATHER CONDITIONS.
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001211X11707 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
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