| Date: | Tuesday 25 September 1984 |
| Time: | 12:30 LT |
| Type: | Cessna T207A |
| Owner/operator: | Air Nevada Leasing I, Inc. |
| Registration: | N75870 |
| MSN: | 20700648 |
| Year of manufacture: | 1980 |
| Total airframe hrs: | 1711 hours |
| Engine model: | Continental TSIO-250-M |
| Fatalities: | Fatalities: 0 / Occupants: 4 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Mexican Hat, UT -
United States of America
|
| Phase: | Approach |
| Nature: | Unknown |
| Departure airport: | Las Vegas, NV (KLAS) |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:PLT STATED AFTER ACCIDENT THAT WHILE ON FINAL APPROACH WITH ENG PWR REDUCED FOR LANDING, THE ACFT BEGAN TO DESCEND BELOW THE DESIRED GLIDEPATH. WHEN THE THROTTLE WAS ADVANCED THERE WAS NO ADDED THRUST. AN IN-FLIGHT RESTART WAS UNSUCCESFUL. THE ACFT LANDED SHORT OF THE RUNWAY AN COLLIDED WITH A DIRT EMBANKMENT. POST CRASH FUNCTIONAL TEST OF THE ENG REVEALED NO EVIDENCE OF A MECHANICAL MALFUNCTION OR FAILURE THAT WOULD PRECLUDE NORMAL ENG OPERATION. THE ENG DID FAIL WHEN THE MIXTURE CONTROL WAS SET FOR SMOOTH ENG OPERATION, THE BOOST PUMP WAS IN THE OFF POSITION AND THE THROTTLE RAPIDLY ADVANCED FROM A LOW PWR SETTING TO FULL PWR.
Probable Cause:
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | DEN84LA299 |
| Status: | Investigation completed |
| Duration: | |
| Download report: | Final report
|
|
Sources:
NTSB DEN84LA299
Location
Revision history:
| Date/time | Contributor | Updates |
| 31-Mar-2024 07:49 |
ASN Update Bot |
Added |
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