ASN Wikibase Occurrence # 38157
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Date: | Thursday 26 September 1996 |
Time: | 23:14 |
Type: | Piper PA-28-180 |
Owner/operator: | Guilford Air Service |
Registration: | N8803J |
MSN: | 28-2751 |
Year of manufacture: | 1965 |
Total airframe hrs: | 4867 hours |
Engine model: | Lycoming O-360-A3A |
Fatalities: | Fatalities: 1 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Birmingham, AL -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Greensboro, NC (W88) |
Destination airport: | (BHM) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot used 8 gallons per hour fuel consumption for the the planned 4-hour flight, with enough fuel for 5 hours. About midpoint of the flight the flight descended to 6,000 feet from the planned 8,000 feet per the pilots request. Slight vectoring was required during the flight for weather avoidance. The passenger reported that when the flight was near the destination, the pilot observed that the fuel gauges were indicating empty, but after observing the city lights near the destination airport he elected to continue the flight. While being vectored onto final approach for a localizer approach the engine experienced a total loss of engine power due to fuel exhaustion. During the forced landing to a highway the airplane collided with unmarked power lines and a vehicle. The right rear seat passenger was ejected from the airplane during the impact sequence. A 2 foot by 2 foot fuel stain on the ground was noted beneath the left wing fuel tank, and 8 ounces of fuel were drained from the right wing fuel tank. Examination of the carburetor revealed worn material on the float needle valve, that the float adjustment was out of limits, and that the economizer jet was improperly adjusted. Examination of the right rear seat cable assembly revealed the swaged fitting was separated and not located. Corrosion and wear was not noted on the cable and the cable strands exhibited evidence of tensile overstress failure. Review of the aircraft logbooks revealed the carburetor was last overhauled in 1967, and was installed in January 1968. The engine was overhauled in 1976, but the carburetor had not been overhauled since 1967. A non-mandatory service bulletin requires carburetor overhaul every 10 years or when the engine is overhauled, whichever occurs first. CAUSE: The pilot-in-command's improper in-flight planning/decision for electing to continue the flight after observing that the fuel gauges indicated empty. Contributing to the accident was an improperly adjusted economizer jet and an out of adjustment float. Also contributing to the accident was unsuitable terrain encountered during the forced landing.
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001208X06784
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
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