| Date: | Tuesday 24 May 1983 |
| Time: | 13:55 LT |
| Type: | Aerospatiale SA 315B Lama |
| Owner/operator: | Airwest Helicopters, Inc. |
| Registration: | N90706 |
| MSN: | 2365 |
| Total airframe hrs: | 4897 hours |
| Engine model: | TURBOMECA ARTOUSTE IIIB |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Fillmore, UT -
United States of America
|
| Phase: | Taxi |
| Nature: | Unknown |
| Departure airport: | |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WHILE ENGAGED IN SEISMIL WORK, THE PLT WAS CONTACTED BY RADIO & WAS ASKED TO ASSIST IN FREEING 2 CREW TRUCKS THAT HAD GOTTEN STUCK IN SAND DUNES. HE DECIDED TO ASSIST SINCE THE STUCK TRUCKS WERE DELAYING THE ENTIRE OPERATION. HE PLANNED TO PARTIALLY RAISE & PULL ONE END OF A TRUCK BY USING A 100 FT LONG LINE. THE HELICOPTER WAS FACING THE AFT END OF THE TRUCK & LONG LINE WAS AT ABOUT A 25-30 DEG ANGLE WHEN CONTINUOUS COLLECTIVE POWER WAS APPLIED. BY THE PLT. THE HELICOPTER THEN YAWED LEFT. THE PLT ATTEMPTED TO COMPENSATE WITH RIGHT ANTI-TORQUE PEDAL, REDUCED POWER & INDUCED RIGHT FORWARD CYCLIC. REPORTEDLY, THE HELICOPTER THEN TURNED 360 DEG & CAME TO REST ON ITS RIGHT SIDE. AT SOME POINT AFTER THE LEFT YAW, THE PLT RELEASED THE LONG LINE. THE COMPANY SAFETY OFFICER REPORTED THAT IF A 150 FT LONG LINE HAD BEEN USED, THERE WOULD HAVE BEEN A LARGER MARGIN FOR ERROR.
Probable Cause:
Accident investigation:
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| | |
| Investigating agency: | NTSB |
| Report number: | DEN83LA118 |
| Status: | Investigation completed |
| Duration: | |
| Download report: | Final report
|
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Sources:
NTSB DEN83LA118
Location
Revision history:
| Date/time | Contributor | Updates |
| 02-Apr-2024 08:27 |
ASN Update Bot |
Added |
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