| Date: | Sunday 3 October 1982 |
| Time: | 10:45 LT |
| Type: | Beechcraft A36TC |
| Owner/operator: | Crown Development Company |
| Registration: | N66909 |
| MSN: | EA-49 |
| Year of manufacture: | 1979 |
| Total airframe hrs: | 503 hours |
| Engine model: | Continental TSIO-520-UB |
| Fatalities: | Fatalities: 0 / Occupants: 3 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Santa Ana, CA -
United States of America
|
| Phase: | Initial climb |
| Nature: | Private |
| Departure airport: | Santa Ana, CA (KSNA) |
| Destination airport: | Oxnard, CA (KOXR) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT REPORTED THAT THE ENGINE LOST POWER AFTER HE HAD RAISED THE GEAR DURING TAKEOFF. HE LOWERED THE NOSE TO AVOID A STALL AND LANDED GEAR-UP AT AND OFF THE END OF THE RUNWAY. REPORTEDLY, TOWER PERSONNEL OBSERVED BLACK SMOKE TRAILING FROM THE BOTTOM OF THE ENGINE COWLING. THE FRONT SEAT PASSENGER, A RATED PILOT, REPORTED THAT THE FUEL PRESSURE NEEDLE WAS PEGGED TO THE HIGH LIMIT. THE PILOT REPORTED THAT THE FUEL FLOW NEEDLE HAD GONE FROM THE 6 O'CLOCK POSITION (36 GPH) TO ABOUT THE 10 TO 11 O'CLOCK POSITION. THERE WAS A HISTORY OF FUEL PRESSURE DISCREPANCIES. THREE FUEL PUMP REPLACEMENTS WERE DOCUMENTED IN THE AIRCRAFT LOGBOOKS. A CHECK OF THE FUEL PUMP REVEALED DISCREPANCIES IN THE FUEL PRESSURE AND FUEL FLOW, BUT THESE INVOLVED LOW OUTPUT RATHER THAN HIGH OUTPUT.
Probable Cause:
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | LAX83LA007 |
| Status: | Investigation completed |
| Duration: | 1 year |
| Download report: | Final report
|
|
Sources:
NTSB LAX83LA007
Location
Revision history:
| Date/time | Contributor | Updates |
| 02-Apr-2024 21:57 |
ASN Update Bot |
Added |
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