| Date: | Friday 1 October 1982 |
| Time: | 15:00 LT |
| Type: | Beechcraft 35-C33 Debonair |
| Owner/operator: | Home Aviaton, Inc. |
| Registration: | N8944U |
| MSN: | CD-954 |
| Total airframe hrs: | 4097 hours |
| Engine model: | Continental IO-470K |
| Fatalities: | Fatalities: 0 / Occupants: 4 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Lake City, FL -
United States of America
|
| Phase: | Landing |
| Nature: | Executive |
| Departure airport: | Gainesville, FL (KGNV) |
| Destination airport: | Greenville, SC (KGMU) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WHILE ENROUTE, THE PILOT DIVERTED TO LAKE CITY, FL TO AVOID ADVERSE WEATHER. ACCORDING TO THE PILOT, HE PLACED THE LANDING GEAR HANDLE IN THE DOWN POSITION WHILE ON THE DOWNWIND LEG. HE EXTENDED THE DOWNWIND TO ACCOMMODATE OTHER TRAFFIC, THEN TURNED BASE AND FINAL WHERE HE COMPLETED THE BEFORE-LANDING CHECKLIST. THE AIRCRAFT WAS LANDED WITH THE GEAR IN ITS RETRACTED POSITION. LATER WHEN THE AIRCRAFT WAS LIFTED, A MECHANIC ACTIVATED THE ELECTRICAL MASTER SWITCH AND MOVED THE GEAR HANDLE TO THE DOWN POSITION. WHEN HE DID THIS, THE GEAR EXTENDED AND THE 3 GREEN LIGHTS ILLUMINATED.
Probable Cause:
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | MIA83LA004 |
| Status: | Investigation completed |
| Duration: | 1 year |
| Download report: | Final report
|
|
Sources:
NTSB MIA83LA004
History of this aircraft
Other occurrences involving this aircraft
| 1 February 2012 |
N331DP |
Mac Air Inc |
0 |
Wallace, NC |
 |
unk |
| 22 August 2012 |
N331DP |
Mac Air Inc |
0 |
Burlington Alamance Regional Airport, NC (KBUY) |
 |
sub |
| Heavy landing |
Revision history:
| Date/time | Contributor | Updates |
| 02-Apr-2024 22:10 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation