| Date: | Saturday 4 September 1982 |
| Time: | 14:04 LT |
| Type: | Piper 601P |
| Owner/operator: | H. Joe Meheen |
| Registration: | N3642Y |
| MSN: | 61P-08298163 |
| Total airframe hrs: | 836 hours |
| Engine model: | Lycoming IO-540-SIA5 |
| Fatalities: | Fatalities: 0 / Occupants: 3 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Burbank, CA -
United States of America
|
| Phase: | Take off |
| Nature: | Private |
| Departure airport: | Burbank, CA (KBUR) |
| Destination airport: | San Carlos, CA (KSQL) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING LIFT-OFF THE RIGHT ENGINE FAILED. THE TAKEOFF WAS ABORTED & THE PLT SWERVED THE ACFT TO AVOID A BLAST FENCE AT THE END OF THE RWY. THE LEFT MAIN LANDING GEAR FAILED & THE ACFT COLLIDED WITH THE FENCE. MAINTENANCE RECORDS REVEALED A TOTAL OF 12 DISCREPANCIES PERTAINING TO FUEL FLOW ON THE RIGHT ENG BEGINNING 7/14/81. AN ENGINE RUN WAS MADE AFTER THEACCIDENT. WHEN TAKEOFF POWER WAS APPLIED & THE BOOST PUMP WAS TURNED ON, THE ENG QUIT. THE RIGHT ENG-DRIVEN FUEL PUMP, LEAR RG 17980J, WAS THEN BENCH TESTED. THE FUEL PUMP COVER DID NOT APPEAR TO BE PROPERLY SAFETY-WIRED. FUEL LEAKED FROM THE VENT HOLE IN THE CAP DURING PRESSURE TESTING. WHEN THE COVER WAS REMOVED, THE DIAPHRAGM RETAINING NUT FELL OUT ONTO THE TEST BENCH.
Probable Cause:
Accident investigation:
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| | |
| Investigating agency: | NTSB |
| Report number: | LAX82DA331 |
| Status: | Investigation completed |
| Duration: | 1 year |
| Download report: | Final report
|
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Sources:
NTSB LAX82DA331
Location
Revision history:
| Date/time | Contributor | Updates |
| 03-Apr-2024 00:19 |
ASN Update Bot |
Added |
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