| Date: | Wednesday 1 September 1982 |
| Time: | 18:10 LT |
| Type: | Rutan VariEze |
| Owner/operator: | Private |
| Registration: | N78EV |
| MSN: | RAF 1803 |
| Total airframe hrs: | 46 hours |
| Engine model: | Continental O-200A |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Palo Alto, CA -
United States of America
|
| Phase: | Approach |
| Nature: | Private |
| Departure airport: | Rialto, CA (L67) |
| Destination airport: | Burbank, CA |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING FINAL APPROACH THE ACFT SUDDENLY PITCHED DOWN ABOUT 45 DEG & CRASHED INTO A DUCK POND CONTAINING APPROXIMATELY 4-5 FT OF WATER. DURING EXAMINATION OF THE WRECKAGE IT WAS NOTED A BOLT WAS MISSING THAT SECURES THE ELEVATOR CONTROL STICK, AT THE BELLCRANK, TO THE PUSH-PULL ROD THAT EXTENDS TO & OPERATES THE ELEVATORS ATTACHED TO THE CANARD. THE PLT STATED THAT PRIOR TO THIS FLT HE HAD PUT IN A NEW INSTRUMENT PANEL DURING WHICH THE CANARD HAD BEEN REMOVED. HE COULD NOT REMEMBER TORQUING THE NUT ATTACHING THE ELEVATOR PUSH-PULL ROD TO THE BELLCRANK WHEN HE REINSTALLED THE CANARD.
Probable Cause:
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | LAX83FVM03 |
| Status: | Investigation completed |
| Duration: | 1 year |
| Download report: | Final report
|
|
Sources:
NTSB LAX83FVM03
Location
Revision history:
| Date/time | Contributor | Updates |
| 03-Apr-2024 00:39 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation