ASN Wikibase Occurrence # 38465
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Date: | Thursday 22 December 1994 |
Time: | 13:52 LT |
Type: | Piper PA-46-350P Malibu Mirage |
Owner/operator: | Ryders Replica Fighter Museum |
Registration: | N133MA |
MSN: | 4622133 |
Total airframe hrs: | 106 hours |
Engine model: | Lycoming TIO-540-AE2A |
Fatalities: | Fatalities: 3 / Occupants: 3 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Rochester, MN -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | |
Destination airport: | Guntersville, AL (8A1 |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRPLANE DEPARTED ON RUNWAY 31 IN INSTRUMENT METEOROLOGICAL CONDITIONS (IMC) AND TURNED RIGHT TO A HEADING OF 090 DEGREES. RADAR CONTACT (ARTS TAG) WAS ACQUIRED ABOUT 1 TO 2 MILES NORTH OF THE AIRPORT. REPORTEDLY, THE ARTS TAG WOULD TYPICALLY BE ACQUIRED AS THE AIRPLANE CLIMBED THROUGH AN ALTITUDE OF ABOUT 700 FEET AGL. SUBSEQUENTLY, THE AIRPLANE CRASHED ABOUT 2 MILES NORTH OF THE AIRPORT. A WITNESS REPORTED HEARING A LOUD ENGINE NOISE BEFORE THE PLANE CRASHED. THE WRECKAGE PATH WAS ORIENTED ALONG A WESTERLY HEADING AND OVER AN AREA OF ABOUT 380 FEET. THERE WAS EVIDENCE OF AN IN-FLIGHT BREAKUP. AN OUTBOARD PORTION OF THE RIGHT WING WAS FOUND ABOUT 150 FEET FROM THE MAIN IMPACT CRATER. AN EXAMINATION REVEALED THE RIGHT WING HAD FAILED NEAR THE PRODUCTION SEAM. THE RIGHT SPAR EXHIBITED FEATURES 'TYPICAL OF AN UPWARD BENDING OVERSTRESS SEPARATION.' EXAMINATION REVEALED NO OTHER EVIDENCE OF PREIMPACT AIRCRAFT OR ENGINE MALFUNCTION. THE AIRPLANE'S GROSS WEIGHT WAS ESTIMATED TO BE ABOUT 4696 POUNDS; ITS MAX LIMIT WAS 4300 POUNDS. THE PILOT'S LOGBOOK INDICATED THAT HE HAD FLOWN ONLY 2 INSTRUMENT APPROACHES IN THE PREVIOUS 14 MONTHS.
Probable Cause: FAILURE OF THE PILOT TO MAINTAIN CONTROL OF THE AIRPLANE, WHILE CLIMBING IN INSTRUMENT METEOROLOGICAL CONDITIONS (IMC) AFTER TAKEOFF. FACTORS RELATED TO THE ACCIDENT WERE: FOG, LOW CEILING, THE PILOT'S LACK OF RECENT INSTRUMENT EXPERIENCE, AND THE EXCESSIVE GROSS WEIGHT OF THE AIRPLANE.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI95FA061 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB CHI95FA061
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
09-Apr-2024 17:42 |
ASN Update Bot |
Updated [Time, Other fatalities, Destination airport, Source, Narrative, Category, Accident report] |
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