| Date: | Thursday 25 March 1982 |
| Time: | 15:25 LT |
| Type: | Beechcraft 58 Baron |
| Owner/operator: | Gapway Groves, Inc. |
| Registration: | N3707N |
| MSN: | TJ320 |
| Total airframe hrs: | 242 hours |
| Engine model: | Continental TSIO-520-WB |
| Fatalities: | Fatalities: 0 / Occupants: 4 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Ridgeland, SC -
United States of America
|
| Phase: | Landing |
| Nature: | Private |
| Departure airport: | Winter Haven, FL (KGIF) |
| Destination airport: | Buckhannon, WV |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT STATED THAT DURING LANDING, THE LEFT BRAKE WAS INOPERATIVE. WHEN HE REALIZED THE PROBLEM, THERE WAS INSUFFICIENT RUNWAY REMAINING TO STOP OR GO-AROUND. AT THE END OF THE RUNWAY WAS A DEEP DROP-OFF. THEREFORE THE PILOT USED THE RIGHT BRAKE, AND SUBSEQUENTLY, THE PLANE DEPARTED THE RIGHT SIDE OF THE RUNWAY. THE RIGHT GEAR SEPARATED IN SOFT TERRAIN AS THE PLANE ENTERED A DEPRESSION BESIDE THE RUNWAY. AN EXAMINATION REVEALED THE LEFT BRAKE MASTER CYLINDER WAS WET WITH HYDRAULIC FLUID. THE CYLINDER, PARAMOUNT MODEL VI-15-750-3, WAS DISASSEMBLED. AN INSPECTION OF THE MASTER CYLINDER PISTON SHAFT REVEALED SEVERAL COMPRESSION INDENTATIONS. THE INDENTATIONS WERE LOCATED IN SUCH A MANNER AS TO PERMIT FLUID LEAKAGE AND INTRODUCTION OF AIR INTO THE CYLINDER. THE CAUSE OF THE INDENTATIONS WAS NOT DETERMINED.
Probable Cause:
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | ATL82DA084 |
| Status: | Investigation completed |
| Duration: | 1 year |
| Download report: | Final report
|
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Sources:
NTSB ATL82DA084
Location
Revision history:
| Date/time | Contributor | Updates |
| 03-Apr-2024 14:41 |
ASN Update Bot |
Added |
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