| Date: | Tuesday 16 January 2001 |
| Time: | 10:15 LT |
| Type: | Lake LA-4-200 |
| Owner/operator: | George Kirby |
| Registration: | N12E |
| MSN: | 932 |
| Total airframe hrs: | 2160 hours |
| Engine model: | Lycoming IO360 A1B6 |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | Orlando, FL -
United States of America
|
| Phase: | Standing |
| Nature: | Private |
| Departure airport: | Orlando Executive Airport, FL (ORL/KORL) |
| Destination airport: | Orlando Executive Airport, FL (ORL/KORL) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was attempting to start the engine when an explosion occurred. He stated that he did not detect any fumes prior to engine start. A crack was found on a fuel block drain assembly fitting and corrosion of the battery grounding strap was also discovered. Maintenance inspection procedures for the airplane requires a 30 day inspection of both the battery grounding strap for corrosion and the fuel lines for damage.
Probable Cause: THE OTHER MAINTENANCE PERSONNEL'S FAILURE TO COMPLETE PRESCRIBED INSPECTIONS THAT RESULTED IN THE FAILURE OF A FUEL BLOCK DRAIN ASSEMBLY FITTING , CORROSION OF THE BATTERY GROUNDING STRAP AND THE SUBSEQUENT FLASH EXPLOSION.
Accident investigation:
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| | |
| Investigating agency: | NTSB |
| Report number: | ATL01LA022 |
| Status: | Investigation completed |
| Duration: | 7 months |
| Download report: | Final report
|
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Sources:
NTSB ATL01LA022
Location
Revision history:
| Date/time | Contributor | Updates |
| 05-Apr-2024 13:24 |
ASN Update Bot |
Added |
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