Accident Mooney M20F N377X,
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ASN Wikibase Occurrence # 38671
 
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Date:Saturday 29 August 1998
Time:16:55 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20F
Owner/operator:R.c. Fugate Enterprises
Registration: N377X
MSN: 670360
Year of manufacture:1967
Total airframe hrs:1053 hours
Engine model:Lycoming IO-360-A1A
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Fort Collins, CO -   United States of America
Phase: Approach
Nature:Private
Departure airport:Chadron, NE (KCDR)
Destination airport:(3V5)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot was returning from a cross-country flight and was observed by witnesses to enter the traffic pattern downwind at an estimated 450 feet agl and very close to the runway. One witness reported that when the aircraft turned base it 'appeared to be a kind of wing-over maneuver.' Another witness said that he 'turned left to the base leg of an approach to runway 11, and [he] quickly increased the bank so that in less than five seconds I could see a full plan view of the airplane at an altitude of approximately 200 feet.' Post-accident investigation indicated that the airplane's bank angle was approximately 30 degrees to the left and 30 degrees nose down upon ground impact. The airport (elevation 4,935 feet, density altitude 7,844 feet) had a local published traffic pattern altitude of 800 feet agl. Post-accident examination of the airplane's altimeter revealed a Kollsman Window setting of 29.96 inches. The closest recorded weather station (7 nautical miles distant and 81 feet above the destination airport elevation) was reporting a barometric pressure of 30.21 inches of mercury. The pilot's altimeter read approximately 250 feet higher than the airplane's actual altitude.

Probable Cause: The pilot's inadvertent stall/mush due to his excessive angle of bank during his traffic pattern turn to base. Factors were the pilot's improper downwind altitude, the pilot not properly setting his Kollsman Window in his altimeter, and the high density altitude.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW98FA378
Status: Investigation completed
Duration: 1 year and 7 months
Download report: Final report

Sources:

NTSB FTW98FA378

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
06-Apr-2024 10:38 ASN Update Bot Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

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