| Date: | Tuesday 14 March 2000 |
| Time: | 17:20 LT |
| Type: | Beechcraft 58 Baron |
| Owner/operator: | Flight Express Inc. |
| Registration: | N225TA |
| MSN: | TH-64 |
| Year of manufacture: | 1970 |
| Total airframe hrs: | 4304 hours |
| Engine model: | Continental IO-520-CB7 |
| Fatalities: | Fatalities: 0 / Occupants: 1 |
| Other fatalities: | 0 |
| Aircraft damage: | Minor |
| Category: | Serious incident |
| Location: | Memphis, TN -
United States of America
|
| Phase: | Landing |
| Nature: | Unknown |
| Departure airport: | Ft. Smith, AR (KFSM) |
| Destination airport: | (KMEM) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that during the landing rollout the right main landing gear collapsed, and the airplane exited the runway. Company maintenance personnel examined the right gear and found that a dynamic brake relay, which provides a momentary surge of reverse current to the right main landing gear for positive stopping was defective. This defective part allowed the motor to drive the gearbox past prescribed limits, inducing a bend into the right main landing gear connecting rod. Once gear down was selected, the rod was placed under a compression load, which caused it to bend even further, and not extend the gear.
Probable Cause: failure of the right main landing gear's dynamic brake relay, that resulted in the motor driving the gearbox past prescribed limits, resulting in a bent connecting rod, and failure of the gear to extend.
Accident investigation:
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|
| | |
| Investigating agency: | NTSB |
| Report number: | MIA00IA104 |
| Status: | Investigation completed |
| Duration: | 1 year |
| Download report: | Final report
|
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Sources:
NTSB MIA00IA104
Location
Revision history:
| Date/time | Contributor | Updates |
| 03-May-2024 10:25 |
ASN Update Bot |
Added |
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