ASN Wikibase Occurrence # 38812
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 30 August 1987 |
Time: | 08:30 |
Type: | Beechcraft B35 Bonanza |
Owner/operator: | private |
Registration: | N700T |
MSN: | D-5916 |
Total airframe hrs: | 4283 hours |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Martinsville, IN -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Martinsville, IN (6I9) |
Destination airport: | Rough River, KY (213) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:SHORTLY AFTER TAKEOFF AN ENGINE FAILURE OCCURRED. THE AIRCRAFT STALLED AND SPUN TO THE GROUND WHEN THE PILOT TRIED TO RETURN TO THE AIRPORT. THE FUEL SELECTOR WAS POSITIONED ON THE ALMOST EMPTY AUXILIARY TANK (MEANT FOR USE IN LEVEL FLIGHT ONLY). CAUSE:
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001213X31744 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation